Form 1 NATIONAL RAILROAD ADJUSTbENT BOARD Award No.
7566
SECOND DIVISION Docket No.
7494
2-WP-MA-'78
The Second Division consisted of the regular members and in
addition Referee Arthur T. Van Wart when award was rendered.
( International Association of Machinists and
( Aerospace Workers
Parties to Dispute:
( Western Pacific Railroad Company
Dispute: Claim of Employes:
1. That under the current Agreement Machinist C. F. Flynn
(hereinafter referred to as Claimant) was improperly suspended
from service for five
(5)
working days commencing on February
23, 1976.
2.
That, accordingly, the Carrier be ordered to compensate Claimant
for wage loss resulting from improper five
(5)
day suspension.
Findings:
The Second Division of the Adjustment Board, upon the whole record and
all the evidence, finds that:
The carrier or carriers and the employe or employes involved in this
dispute are respectively carrier and employe within the meaning of the
Railway Labor Act as approved June
21, 1934.
This Division of the Adjustment Board has jurisdiction over the dispute
involved herein.
Parties to said dispute waived right of appearance at hearing thereon.
Claimant Machinist, on November
25, 1975,
was working the position of
Locomotive Inspector at Carrier's Diesel Shop at Stockton, California. The
duties of such position required, among other things, that Claimant make
various inspections, on Locomotives, including inspection for fuel leaks.
Locomotive
WP
3521
was brought into said shop and placed over the pit
during Claimant's tour of duty on November
25, 1975.
Claimant inspected said
Locomotive and signed Form
2-A,
Locomotive Inspection Report, attesting
that he had checked said locomotive for fuel leaks.
Locomotive
3521
remained at Stockton until
7:50
a.m. November
26,
1975
at which time it was placed on eastbound Main "APRG". Train APRG
arrived at Orville, 111 miles away, on the main line at
11:40
a.m. at which
time a F-decal Locomotive Inspector made an inspection of the train's
Locomotive. His inspection revealed a fuel leak for which said Inspector
filed a "Special Notice for Repairs" causing Engine
3521
to be removed from
service at Orville and returned to Stockton for repairs.
Form 1 Award No.
7566
Page
2
Docket No.
7494
2-WP-MA-'78
Claimant was notified to attend an investigation to ascertain the
facts and determine his responsibility, if any, for his failure to find
and report leak in fuel tank of Unit
WP-354
which he had inspected
Tuesday., Noveriner
25, 1973.
As a result of the investigation held thereon
Claimant was adjudged to have failed to locate and report a leak that
existed in the fuel tank of Unit
WP-354.
Claimant was assessed five
(5)
working days as discipline for such failure.
In the absence of any question on alleged procedural error the merits
of the case are addressed. It is held that there was sufficient evidence
adduced at the investigation to support the conclusions reached by Carrier
as to the Claimant's culpability. The basic defense raised on behalf of
Claimant, to wit, that Foreman Skinner had been negligent, even if true,
would not provide a basis for exculpating claimant. Claimant was paid for
being Carrier's Locomotive Inspector on November
25, 1975.
As such, he was
charged with the responsibility, among other things, to inspect Engine
3521
for fuel leaks and to record the findings of his inspection on
Form
2-A.
The absence of any notation on Form 2-A, indicating that fuel
leaks were discovered on the engine inspected, in the light of the evidence
adduced, is construed to represent an ommission on the part of Claimant.
It has been long recognized that the dereliction of duty by one employee
does not serve to excuse the failure of another employee to properly
perform his duties. As was pointed out by this Division in its Award
3840
(Doyle):
"The fact that others, including possibly the foreman,
may have also been negligent does not excuse the
conduct of Claimants. The standard of reasonable
prudence remains constant and is not lowered by
reason of the fact that there may be general
laxity."
Similarly Award
1716
also held:
"Every employee is responsible for the performance of
his duties and, if he fails to properly perform them
he cannot excuse himself from his responsibility
for such failure merely because others may have been
guilty of the samie fault."
The discipline assessed, in the circumstances herein, was not
unreasonable.
A W A R D
Claim denied.
Form 1
Page
3
Award No.
7566
Docket No.
7494
2-WP-MA-'78
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Second Division
Attest: Executive Secretary
National Railroad Adjustment Board
By _ - n-ct-.z--~- J~/L-~-~--~`- L~
o,emarie Brasch - Administrative Assistant
Dated a Chicago, Illinois, this 16th day of June, 1978.