Form 1 NATIONAL RAILROAD ADJUSTMENT BOARD Award No. 10203
SECOND DIVISION Docket No. 10181
2-IHB-MA-' 85
The Second Division consisted of the regular members and in
addition Referee Hyman Cohen when award was rendered.
( International Association of Machinists
( and Aerospace Workers, AFL-CIO
Parties to Dispute:
(Indiana Harbor Belt Railroad Company
Dispute: Claim of Employes:
1. That the Indiana Harbor Belt Railroad Company be ordered to restore
Machinist D. Spriggs to service and compensate him for all wages lost during
this period to restoration, at the prevailing Machinist rate of pay.
2. That machinist D. Spriggs be restored to service with seniority unimpaired
and compensated for all insurance benefits, vacation benefits, holiday benefits
and any other benefits that may have accrued and were lost, in accordance with
Rule 36 of the agreement effective January 1, 1947 as subsequently amended.
FINDINGS:
The Second Division of the Adjustment Board, upon the whole record and all
the evidence, finds that
The carrier or carriers and the employe or employes involved in this dispute
are respectively carrier and employes within the meaning of the Railway Labor
Act as approved June 21, 1934.
This Division of the Adjustment Board has jurisdiction over the dispute
involved herein.
Parties to said dispute waived right of appearance at hearing thereon.
The Claimant was a machinist Inspector at the Carrier's Gibson Enginehouse
with a service date of June 23, 1976. An investigation was held on October 13,
1981 based upon the following charge:
"On September 23, 1981 you failed to properly perform your assigned
duties on unit 8824 and falsified-company and Federal documents."
As a result of the investigation, the Claimant was dismissed from the service
of the Carrier, effective October 22, 1981.
On September 23, 1981, the Claimant was assigned to change airbrake equipment
on unit 8824. He admitted that he did not inspect the locomotive for a 02YO
(24-month) airbrake test in accordance with Federal Railroad Administration
regulations. The Claimant also acknowledged that he did not change the airbrake
equipment on the unit. He explained that at the storehouse, he
"found
all we
could change was the transfer valve, the independent
[and]
the blanking plate
gasket **" and that he changed the gaskets because this was the only equipment
available to him. However, the Claimant's signature appears on the Carrier and
Federal forms certifying that the 24-month airbrake inspection had been conducted
in accordance with the regulations. Dnginehouse Foreman Jeffrey Barks went to
the Storehouse the morning after the incident and found that it had all of the
necessary materials for the 2Y and the airbrake equipment for unit 8824.
Form 1 Award No. 10203
Page 2 Docket No. 10181
2-IHB-XA-185
Contrary to the Organization's contention, the charge was adequate to inform
the Claimant of the matter to be investigated. Indeed, the record discloses
that before the
investigation notice
was sent to the Claimant, he was aware
that the Carrier might "hold an
investigation" concerning
his conduct on September
23, 1981. Moreover, it is not essential that the Claimant's supervisor, who
had resigned, was not present as a witness at the investigation. Even assuming,
as the Organization contends, that the Claimant's supervisor knew that he had
not completed the required work and permitted him to sign forms certifying to
the contrary, (and there is no proof to that effect), the Claimant is not exonerated
from committing such a serious offense. Moreover, the Board is persuaded that
the used gaskets exhibited at the investigation were from unit 8824 and were
e
not deliberately taken off another unit by the Carrier in order to support the
charges against the Claimant.
The Claimant's record was properly submitted at the investigation for the
purpose of determining the degree of discipline rather than to prove the Claimant's
guilt
concerning his
conduct on September 23, 1981. In roughly over five (5)
years of employment with the Carrier, the Claimant's record contains disciplinary
suspension for offenses, ranging from insubordination, and leaving the service
of the Carrier, to excessive absenteeism.
The Board is persuaded that the Carrier carried its burden of proving that
on September 23, 1981, the Claimant failed to properly perform
his
assigned
duties on unit 8824 and falsified both Carrier and Federal documents. In light
of the Claimant's past disciplinary record, the Board concludes that there is
no basis for disturbing the penalty of dismissal.
A W A R D
Claim denied.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Second Division
Attest:
Nancy J. v4?r-Executive Secretary
Dated at Chicago, Illinois, this 9th day of January 1985.