Form 1 NATIONAL RAILROAD ADJUSTMENT BOARD Award No. 11439
SECOND DIVISION Docket No. 11161
88-2-85-2-308
The Second Division consisted of the regular members and in
addition Referee Elliott H. Goldstein when award was rendered.
(International Association of Machinists and
( Aerospace Workers, AFL-CIO
PARTIES TO DISPUTE:
(Consolidated Rail Corporation
STATEMENT OF CLAIM:
1. That the Consolidated Rail Corporation be ordered to remove the
fifteen (15) day suspension from the record of Machinist R. Lento.
2. That the Consolidated Rail Corporation be ordered to compensate
Machinist R. Lento for all lost time at the applicable machinist rate of pay,
due to the suspension in accordance with rule 7-A-1 (e) of the May 1, 1979
Agreement.
3. The Agreement of May 1, 1979 was controlling.
FINDINGS:
The Second Division of the Adjustment Board upon the whole record and
all the evidence, finds that:
The carrier or carriers and the employe or employes involved in this
dispute are respectively carrier and employes within the meaning of the
Railway Labor Act as approved June 21, 1934.
This Division of the Adjustment Board has jurisdiction over the
dispute involved herein.
Parties to said dispute waived right of appearance at hearing thereon.
Claimant entered Carrier's service on June 13, 1969. On November lfi,
1983 and December 21, 1983, Claimant was present at an Investigation on the
charge that he improperly inspected Unit 3178 on or about September 7, 1983
"...which resulted in premature failure and removal of Number 3 traction motor
and wheel assembly on September 24, 1983." Following the Hearing, Claimant
was assessed a fifteen day deferred suspension.
At the Hearing, Carrier's Superintendent of Motor Power testified
that on September 24, 1983, Locomotive Unit 3178, Train TV 14, was set off at
Beacon Park Diesel Facility due to a continuous wheel slip. The cause of the
locomotive failure was traced to an improperly secured gear case, resulting in
loss of gear case lubricant, excessive wear to the #3 pinion gear and the
improper operation of the #3 wheel armature.
Form 1 Award No. 11439
Page 2 Docket No. 11161
88-2-85-2-308
The record also establishes that the locomotive in question was
shopped at Selkirk Diesel Terminal on September 7 and 8, 1983, for an annual
inspection. This periodic maintenance included inspection of all locomotive
truck components, journal boxes, and wheels. Claimant performed this inspection, and in his signed report did not make reference to a defect of the
nature described above.
Carrier asserts that had the Claimant performed the inspection properly, the improperly secured gear case would have been noted and corrective
action taken, thereby preventing the wheel malfunction that caused the locomotive failure. After careful review of the record evidence in its entirety,
however, the Board finds lacking the substantial evidence necessary to prove
the charges against Claimant. Essentially, the Carrier's claim is one of
improper or substandard work performance - negligence on the part of the
Claimant. Yet, the Carrier never offered proof to support two crucial aspects
of a negligence claim. Absent here is the necessary evidence that Claimant's
inspection was less than adequate or complete. In addition, Carrier did not
prove the second element of negligence: that Claimant's inspection was the
proximate cause of the locomotive failure. As the Organization convincingly
showed at the investigation, there were at least several other equally likely
causes for the malfunction, including damage to a gear pan, which might have
unknowingly occurred after the inspection. In short, we must agree with the
Organization that mere surmise and conjecture are not evidence, and where the
Carrier has failed to meet its burden on the essential elements of its
charges, we must rule to sustain the grievance.
A W A R D
Claim sustained.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Second Division
Attest:
Nancy J. er - Executive Secretary
Dated at Chicago, Illinois, this 16th day of March 1988.