Form 1 NATIONAL RAILROAD ADJUSTMENT BOARD Award No. 12133
SECOND DIVISION Docket No. 11871
91-2-89-2-181
The Second Division consisted of the regular members and in
addition Referee Marty E. Zusman when award was rendered.
(International Association of Machinists and Aerospace
( Workers
PARTIES TO DISPUTE:
(National Railroad Passenger Corporation (Amtrak)
STATEMENT OF CLAIM:
1. The National Railroad Passenger Corporation, (Amtrak) violated
Rule 24 of the schedule agreement effective September 1, 1977, when it
arbitrarily and capricously dismissed Chicago Machinist S. Larson following
investigation held on April 21, 1988.
2. Accordingly, the decision should be reversed, Machinist S. Larson
restored to service with all-rights, seniority and benefits unimpaired, made
whole for any and all losses as a result of the decision, and his record
cleared of any reference to the charge.
FINDINGS:
The Second Division of the Adjustment Board upon the whole record and
all the evidence, finds that:
The carrier or carriers and the employe or employes involved in this
dispute are respectively carrier and employes within the meaning of the
Railway Labor Act as approved June 21, 1934.
This Division of the Adjustment Board has jurisdiction over the
dispute involved herein.
Parties to said dispute were given due notice of hearing thereon.
Claimant was assigned to perform maintenance functions. On February
20, 1988, at the completion of his assignment, Claimant signed off as having
properly performed his duties. Claimant initialed the form indicating completion of the renewal of "wicks and wick oil in the traction motor suspension
bearings and lock wire cap screws" of Locomotive No. 386.
By letter dated March 15, 1988, Claimant was notified to attend a
formal Investigation alleging that Locomotive No. 386 was found to have water
present in the support bearing wells, although the work was signed off as
having been completed. After two postponements, an Investigation was held in
absentia on April 21, 1988. Following the Investigation, the Carrier concluded that the Claimant was guilty as charged. The Claimant was dismissed
from the service of the Carrier, effective May 4, 1988.
Form 1 Award No. 12133
Page 2 Docket No. 11871
91-2-89-2-181
The Organization has argued that the Investigation went forth without
further postponement, even though the investigating officer was aware that
unusual circumstances precluded adequate preparation and notice to the Claimant. The Organization further argues that the results of the capricious
Investigation failed to prove that the Claimant was guilty of the alleged
failure to complete his assignment.
The Board's careful review of the Investigation transcript finds
sufficient probative evidence that the Claimant was guilty as charged. The
record indicates that the Claimant was assigned to properly "review wicks and
wick oil for traction motor suspension bearings" for Engine No. 386. Testimony is sufficient to conclude that Claimant did indicate completion of the
work. A Machinist testified that the drain plugs of Engine No. 386 did not
appear to have been removed and that his further inspection found water in
motor numbers three and four. This was confirmed by the Foreman. The Foreman
also testified that the oil was contaminated and the water could have diminished proper lubrication causing a derailment.
The facts of this case clearly support the Carrier's findings of
guilt. The Board's review of the on-property record finds no procedural
errors. An Investigation held in absentia is insufficient to warrant the
conclusion of a Rule violation denying Claimant a fair aid impartial Investigation (Second Division Awards 10343, 9943; Third Division Award 20113).
Having concluded that the Claimant received all of his Agreement protected
rights and that the probative evidence substantiates Carrier's conclusion of
guilt, the only remaining_issue for this Board to consider is the assessed
discipline.
As the Carrier has noted, falsifying a report of work performed has
been found by this Board as warranting dismissal (Second Division Awards 4199,
6546). Employees are expected arid required to perform their work diligently
and to make proper reports to the Carrier. This the Claimant failed to do and
for that there can be no excuse for his wrongdoing. Claimant must know that
falsification of a work report is a serious act of dishonesty for which dismissal is fully justified. Without mitigating guilt, the Board finds the
instant discipline was excessive given the circumstances at bar and the Claimant's past disciplinary record. Claimant is to be returned to service on a
last chance basis with seniority rights and benefits unimpaired, but without
compensation for time lost.
A W A R D
Claim sustained in accordance with the Findings.
Form 1
Page 3
Attest: ~z
Award No. 12133
Docket No. 11871
91-2-89-2-181
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Second Division
000
Nancy J. -Executive Secret ry
Dated at Chicago, Illinois, this 18th day of September 1991.