Form 1 NATIONAL RAILROAD ADJUSTMENT BOARD Award No. 12164
SECOND DIVISION Docket No. 12237
91-2-91-2-23
The Second Division consisted of the regular members and in
addition Referee Hugh Duffy when award was rendered.
(International Association of Machinists and
( Aerospace Workers
PARTIES TO DISPUTE:
(CSX Transportation, Inc. (Former Seaboard Coast
( Line Railroad Company)
STATEMENT OF CLAIM:
1. That CSX Transportation, Inc. violated Rule 30, but not limited
thereto, of the controlling Agreement when it unjustly suspended Machinist J.
J. Overall for thirty days following an investigation held on April 16, 1990.
2. That accordingly, CSX Transportation be ordered to compensate
Machinist Overall for all pay and benefits lost (made whole) as a result
thereof and remove all reference to the charges from his record.
FINDINGS:
The Second Division of the Adjustment Board, upon the whole record
and all the evidence, finds that:
The carrier or carriers and the employe or employes involved in this
dispute are respectively carrier and employes within the meaning of the
Railway Labor Act as approved June 21, 1934.
This Division of the Adjustment Board has jurisdiction over the
dispute involved herein.
Parties to said dispute waived right of appearance at hearing
thereon.
Claimant was charged with violating Rules 250 and 253 of the Safety
Manual, after an unexpected movement of a locomotive he was conducting a test
on caused an injury to another employee. After an Investigation, Claimant was
found guilty as charged and assessed the penalty of a 30-day suspension.
It should be noted at the outset that the Organization raised matters
which were not considered on the property; not having been raised in a timely
manner, they have not been considered in the Board's deliberations.
In this case an Electrician and a Foreman were inspecting the flange
lubricator on a locomotive, requiring that they "fool" the engine by setting
the generator field in the "ON" position, the reverser in the "FORWARD" position, and the isolation switch in the "RUN" position; this enabled them to
simulate running conditions without actually starting the engine.
Form 1 Award No. 12164
Page 2 Docket No. 12237
91-2-91-2-23
While this test was proceeding, Claimant arrived to perform a "break
in two" protection test, which required starting the engine. This meant that
the generator field had to be in the "OFF" position, the reverser in "NEUTRAL", and the isolation switch off the line. Claimant proceeded with the
test but failed to check the position of the reverser, which had been set in
"FORWARD" by the two other employees. This eventually resulted in a forward
movement of the locomotive, causing a minor injury to the Electrician.
After a close review of the transcript, it is clear that Claimant is
culpable for failing to check the position of the reverser, and he cannot
point to the shortcoming of others to justify his failure to devote his full
attention to the task at hand. However, there do appear to be other mitigating factors, and given all the circumstances, suspension for 30 days appears to be an excessive penalty in this case. We therefore conclude that a
10-day suspension would have been more commensurate with what occurred in this
matter. Accordingly, Claimant's suspension would cover the period from May 4,
1990 through May 13, 1990.
A W A R D
Claim sustained in accordance with the Findings.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Second Division
Attest:
Nancy J. er - Executive Secretary
Dated at Chicago, Illinois, this 9th day of October 1991.