Form 1 NATIONAL RAILROAD ADJUSTMENT BOARD Award No. 12437
SECOND DIVISION Docket No. 12491
92-2-92-2-6
The Second Division consisted of the regular members and in
addition Referee Kay McMurray when award was rendered.
(International Brotherhood of Electrical Workers
PARTIES TO DISPUTE
:
(Florida East Coast Railway Company
STATEMENT OF CLAIM:
1. That at New Smyrna Beach Locomotive Shop, on October 24, 1990,
with reference to Electrician J. R. Thompson's formal investigation, Carrier
assessed discipline of twenty (20) days actual suspension, November 7-December
4, 1990. The Florida East Coast Railway Company has violated the controlling
agreement, and particularly Rule 26, Discipline Hearings alleging that formal
investigation conclusively developed that Electrician J. R. Thompson failed to
properly perform his duties when he failed to check AR-10 even by looking
through the glass insert on the cover; for had he done so he would have detected that a wire was burned off a fuse on a buss bar.
2. That Electrician J. R. Thompson be compensated eight (8) hours for
each regular assigned work day beginning November 7 - December 4, 1990, at the
pro rata rate for all lost wages, be made whole for all vacation rights, made
whole for all health and welfare and insurance benefits, made whole for all
pension benefits, including Railroad Retirement and Unemployment Insurance,
and made whole for any other benefits that Claimant would have earned during
the time he was held out of service, and personal record he completely
cleared.
FINDINGS:
The Second Division of the Adjustment Board, upon the whole record
and all the evidence, finds that:
The carrier or carriers and the employe or employes involved in this
dispute are respectively carrier and employes within the meaning of the
Railway Labor Act as approved June 21, 1934.
This Division of the Adjustment Board has jurisdiction over the
dispute involved herein.
Parties to said dispute waived right of appearance at hearing
thereon.
Form 1 Award No. 12437
Page 2 Docket No. 12491
92-2-92-2-6
On July 27, 1990, Diesel Engine 425 was brought to the New Smyrna
Beach Lomocotive Shop for a usual P-12 Inspection. General Foreman, James
Church, assigned the Claimant to the inspection. Mr. Church advised Claimant
that when the locomotive was brought in he made several moves with it and
noticed that the engine overloaded in amperage. Normally, when throttles were
advanced the amperage would read around 200 but the engine on 425 loaded up
rapidly to 500 and 600 amps, causing a very quick take off. This pointed to
an electrical problem and the Foreman verbally described the situation to the
Claimant. He was told to inspect the diodes and fuses and look in the back of
the AR-10 generator. During the inspection period, July 27 - August 1, 1990,
Claimant signed off on the appropriate form indicating that the work had been
accomplished and everything was in order. On August 1, the planned completion date of the inspection, General Foreman, T. N. Iltsopoulos, was moving
Locomotive 425 from #2 pit to the washrack, when he noticed that the amp meter
was higher than normal, about 500-700 amps. He was accompanied in the cab by
another Foreman and the Claimant. He asked the Claimant if he had inspected
the AR-10 main generator for burned fuses and diodes. Claimant responded that
everything is OK in the generator and that he had told everybody concerned.
The Shop Superintendent was then asked to trouble shoot and repair the overloading problem on Locomotive 425. A test, first conducted by Claimant and
then jointly by the Shop Superintendent and the Claimant, failed. Accordingly, the Shop Superintendent, was assigned the task of repairing the overload
problem. Early on the following day, August 2, he inspected the AR-10 - D14
generator assembly and noticed through the inspection window that the dome
wire lugs were burned off. He removed the left inspection cover and found B1,
J2 wire lug and the mounting bolt burned off the left fuse buss bar. The
repairs were completed and the overloading problem was eliminated. The locomotive was returned to service August 2, one day later than planned. Claimant
was charged with failing to properly perform his duties as an Electrician and
following mutually agreed delays the Hearing proceeded on October 24, 1990.
In a timely manner after the Hearing, Claimant was assessed the penalty herein
complained of.
The Organization raises the defense that the Claimant did not receive
a fair and impartial Hearing because of the manner in which the tapes of the
Hearing were transcribed. It notified the company that their information revealed that the transcriber was being assisted by supervisory employees. An
Investigation by the Carrier revealed that the transcriber had in fact asked
two of the witnesses to proofread a portion of their testimony to insure accuracy because the tape was difficult to understand. In order to avoid further
complications, the tapes from this and other Investigations were removed from
New Smyrna to St. Augustine to be transcribed by General Office personnel.
The Carrier refused the Organizations request for an independent transcriber
but did furnish a copy of the transcripts and made the tapes available for
review at the General offices during normal working hours. The Organization
made no effort to review the tapes. Having declined the opportunity to check
the tapes and transcript for accuracy, it cannot now claim that the transcription is inaccurate. We find that the Hearing was conducted in the normal
manner and was fair and impartial.
Form 1 Award No.
12437
Page 3 Docket No. 12491
92-2-92-2-6
The transcript and file in this case is quite voluminous. There are
some diagreements in the testimony of the witnesses. This Board is in no
position to judge the credibility of witnesses and must make its decision on
the credible evidence in the record.
The record reveals that Locomotive 425 came into the inspection site
on July 27. Among its problems was an amperage overload which all parties
agree indicated an electrical problem. Claimant inspected the generator
assembly and found it in working order, signed off on the proper form, and
also verbally informed Supervisors that the work was accomplished. On August
1, the date for the inspection to be completed, the overload problem still
existed. A shop Superintendent was assigned the task of repairing the overload problem. On the morning of August 2, he inspected the generator assembly
and noticed through the window that a problem existed. He removed the left
inspection cover and found the: wire lug and the mounting bolt burned off the
left fuse buss bar. Repairs were made and the locomotive operated properly.
It was released for service that day - one day longer than planned for the
inspection.
From the foregoing and the entire record, we conclude that the Claimant did fail to perform his duties as required by the operation. We also find
the penalty not to be capricious, arbitrary, or overly severe.
A W A R D
Claim denied.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Second Division
Attest: .
cy J. r - Executive Secretary
Dated at Chicago, Illinois, this 23rd day of September 1992.