Form 1 NATIONAL RAILROAD ADJUSTMENT BOARD Award No. 12438
SECOND DIVISION Docket No. 12492
9-2-2-92-2-7
The Second Division consisted of the regular members and in
addition Referee Kay McMurray when award was rendered.
(International Brotherhood of Electrical Workers
PARTIES TO DISPUTE:
(Florida East Coast Railway Company
STATEMENT OF CLAIM:
1. That at New Smyrna Beach Locomotive Shop, on October 24, 1990,
with reference to Electrician J. R. Thompson's, formal investigation, the
Florida East Coast Railway Company assessed discipline of ten (10) days actual
suspension December 5 through December 18, 1990. That Florida East Coast
Railway Company has violated the controlling agreement, and particularly Rule
26, Discipline Hearings, alleging that the preponderance of evidence developed
that Mr. J. R. Thompson simply failed to perform his duties properly, for had
he done so, he would have detected that the ground coil relay wire on the No.
3 traction motor was disconnected and had to be reattached.
2. That Electrician J. R. Thompson be compensated eight (8) hours
for each regular assigned work day beginning December 5 through December 18,
1990, at the pro rata rate for all lost wages, be made whole for all vacation
rights, made whole for all health and welfare and insurance benefits, made
whole for all pension benefits, including Railroad Retirement and Unemployment:
Insurance, and made whole for any other benefits that Claimant would have
earned during the time he was held out of service, and personnel record be
completely cleared.
FINDINGS:
The Second Division of the Adjustment Board upon the whole record and'.
all the evidence, finds that:
The carrier or carriers and the employe or employes involved in this
dispute are respectively carrier and employes within the meaning of the
Railway Labor Act as approved June 21, 1934.
This Division of the Adjustment Board has jurisdiction over the
dispute involved herein.
Parties to said dispute waived right of appearance at hearing thereon..
Form 1 Award No. 12438
Page 2 Docket No. 12492
92-2-92-2-7
On August 7, 1990, the Claimant performed assigned maintenance work
on Locomotive 437 at the New Smyrna Beach Locomotive Shop. Upon completion of
the work, the locomotive was towed to Bowden and then operated as power on
Train 125 from Jacksonville to Miami. It arrived in Miami on August 8, the
following day. Although an occurrence described as a ball of fire emanating
from beneath the locomotive occurred enroute, the maintenance people at
Hialeah were unaware of any problem with the locomotive when it arrived. When
they went to fix the locomotive: on the next train, a ground fault was noticed
on a locomotive attached to Locomotive 437. Both locomotives were then inspected and it was determined that the coil wire was off the ground relay on
Number 3 traction engine on Locomotive 437. Claimant was charged with failing
to perform his duties properly as he should have detected that the coil wire
was off the ground relay. Fol7.owing a Hearing he was assessed the penalty
herein complained of.
The Organization raises the defense that the Claimant did not receive
a fair and impartial Hearing because of the manner in which the tapes of the
Hearing were transcribed. It notified the company that their information
revealed that the transcriber was being assisted by supervisory employees. An
investigation by the Carrier revealed that the transcriber had in fact asked
two of the witnesses to proofread a portion of their testimony to insure
accuracy because the tape was difficult to understand. In order to avoid
further complications, the tapes from this and other investigations were
removed from New Smyrna to St. Augustine to be transcribed by General Office
personnel. The Carrier refused the Organizations request for an independent
transcriber but did furnish a copy of the transcript and made the tapes available for review at the General Offices during normal working hours. The Organization made no effort to review the tapes. Having declined the opportunity to check the tapes and transcript for accuracy, it cannot now claim
that the transcription is inaccurate. We find that the Hearing was conducted
in the normal manner and was fair and impartial.
Claimant testified that on August 7 he took over from another electrician, was briefed by that person on the work he had accomplished and the
proceeded to thoroughly check and repair the problem. He stated that in
addition he looked over the whole locker and the ground relay coil wire was
not disconnected. During the work two Supervisors had inquired regarding
Claimant's progress and he had shown them what he had found and then proceeded
with his repairs. After the work was completed he again showed the Supervisors what he had done and felt they were pleased with his work. The Carrier
does not refute the statement regarding the Supervisors participation. There
seems to be little agreement on what caused the so called ball of fire enroute. The General Diesel Supervisor speculated that the locomotive had a
ground action of some kind. In his testimony he suggested that it might have
been a ground problem or wheel slip. In any event, the train proceeded to its
destination without incident. Nothing in the record proves that it was caused
by Claimant's actions. When queried by the person who conducted the Hearing
if it was possible for the wire to fall off in transit, the Carrier witness
Form 1 Award No. 12438
Page 3 Docket No. 12492
92-2-92-2-7
testified "I really don't know." The General Diesel Foreman who conducted the
inspection at Hialeah testified that the machinist who assisted him megged the
locomotive. It is not clear in the record how many times this was accomplished or at what stage of they inspection the megging was accomplished.
According to the testimony of << Carrier witness, the coil wire is pulled off
the ground relay anytime a megging is conducted. If the inspector followed
proper procedures, the coil wire could have been pulled off the motor during
the inspection.
Locomotive 437 traveled almost 400 miles after Claimant completed his
inspection without incident ati:ributable to Claimant's completed work. To
conclude that the Claimant is guilty as charged the Board would have to deny
all the possibilities inherent in the operation for error on the part of
others associated with this incident. The record simply does not sustain such
a decision.
Based on the foregoing and the entire record we find that the Carrier
did not prove by a preponderance of evidence the Claimant is guilty of the
charge. He is to be paid for all time lost and his record is to be expunged
relative to this matter.
A W A R D
Claim sustained.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Second Division.
Attest:
..(
Nancy J r - Executive Secretary
Dated at Chicago, Illinois, this 23rd day of September 1992.