NATIONAL RAILROAD ADJUSTMENT BOARD
THIRD DIVISION Docket Number CL-19976
Irwin M. Lieberman, Referee
(Brotherhood of Railway, Airline and Steamship Clerks,
( Freight Handlers, Express and Station Employees
PARTIES TO DISPUTE:
(Southern Railway Company
STATEMENT OF CLAIM: Claim of the System Committee of the Brotherhood (GL-7165)
that:
(a) Carrier violated the Clerks' Agreement at Sheffield, Alabama,
when on March 27, 1969, Agent Terminal Control Mr. H. H. Surrett dismissed
Mr. J. G. Everett, Chief Yard Clerk, from the service of the Carrier for
alleged failure to properly handle with Control Center, Atlanta, Georgia, to
obtain billing instructions.
(b) Carrier failed to prove the charges against Mr. Everett in the
investigation held at Sheffield, Alabama, in the office of the Agent Terminal
Control at 3:00 p.m. on April 16, 1969.
(c) Mr. Everett shall be compensated for all time lost, including one
holiday, beginning March 27 through April 30, 1969.
OPINION OF BOARD: Claimant was regularly assigned as Chief Yard Clerk (first
shift) in Carrier's Yard Offices at Sheffield, Alabama. He
had occupied that position for approximately fifteen years and had about 24
years of service with the Carrier. On March 27, 1969 Claimant was dismissed
from service for " ....his failure to properly handle with the Control Center
in Atlanta, Georgia, to obtain billing instructions for tank car GATX 63651..."
which had arrived loaded in the Sheffield Yard on February 19 and remained there
until March 27, 1969 when billing was received. This delay resulted in a serious
complaint from the shipper. After a hearing, the discipline was affirmed by
Carrier. On May 1, 1969, on a leniency basis, Claimant was restored to service,
having lost 24 days (and one holiday) of service.
The record discloses that the car in question had been travelling on
a waybill with an incorrect number. Furthermore, the car had become separated
from that waybill at Birmingham, Alabama, and moved without billing to Sheffield.
The transcript of the investigation indicates that Claimant as well as a number
of other clerks on all three shifts had made dilligent efforts to secure disposition of the car. It
for blame in this matter, particularly since the car in question arrived on the
third shift, prior to his coming on duty.
Award Number 20015 Page 2
Docket Number CL-19976
IE is clear that employee error, compounded, resulted in the inordinate delay of the loaded tank
record that Claimant was not responsible for the mishandling of the car. In
short, the record does not support the conelusion reached by Carrier. A complete examination of the
error committed by Claimant was that he did not handle his tracing with the
Control Center on the proper forms and that he didn't properly log his efforts
and conversations to secure appropriate disposition of the car. Certainly these
minor indiscretions did not warrant the discipline of dismissal or even loss of
twenty five days pay. We shall reduce the discipline to a 10 day suspension.
FINDINGS: The Third Division of the Adjustment Board, after giving the
parties to this dispute due notice of hearing thereon, and upon
the whole record and all the evidence, finds and holds:
That the Carrier and the Employes involved in this dispute are
respectively Carrier and Employes within the meaning of the Railway Labor
Act, as approved June 21, 1934;
That this Division of the Adjustment Board has jurisdiction over
the dispute involved herein; and
That the discipline imposed was excessive.
A WAR D
Discipline reduced to a ten day suspension.
NATIONAL RAILROAD ADJUSTMENT BOARD
4d
Ale
&4/0-0.
By Order of Third Division
ATTEST:
Executive Secretary
Dated at Chicago, Illinois, this 31st day of October 1973.