NATIONAL RAILROAD ADJUSTMENT BOARD
THIRD DIVISION Docket :lumber MW-20241
(Brotherhood of Maintenance of Way Employes
PARTIES TO DISPUTE:
(Louisville and Nashville Railroad Company
STATEMENT OF CLAIM: Claim of the System Committee of the Brotherhood
that:
(1) The Carrier acted improperly, arbitrarily, capriciously,
without just and sufficient cause and on the basis of unproven charges
when it demoted Foreman A. C. Teague and took away his seniority as a
Rank 1 Foreman (System File 1-12/D-104425 E-306-18).
(2) Mr. A. C. Teague's seniority as Rank 1 Foreman be restored and unimpaired and that he be allowed
what he would have received as foreman (including overtime) and what
he was paid in a lower rank position from September 22, 1972 until he
is returned to work as a Rank 1 Foreman.
OPINION OF BOARD: Grievant A. C. Teague was employed by the Carrier
on October 3, 1928, and held seniority as Rank 1
Foreman from October 22, 1946 until demoted on September 22, 1972,
having accumulated some 26 years as Rank 1 Foreman, and 44 years as an
employee with the Carrier. The demotion of Grievant is in issue.
On the morning of September 22, 1972, track foreman Teague
had received instructions to pull a low spot in the main track just
north of a road crossing at Crofton, Kentucky. After Grievant and his
three-man crew had completed this assignment and departed, the Assistant
Division Engineer and Assistant Roadmaster were at the location, as was
also the Assistant Roadmaster who instructed Grievant, and they noticed
a hump in the main track where Grievant had worked. Immediately, it was
decided to have a 25 MPH slow order placed on the track, and after further examination it was decide
rail gang was used that afternoon to correct the section of track. Although there may be some questi
the track had been raised--whether 1" as stated by Grievant or 4-3/4" as
stated by the Assistant Engineer and by the Assistant Roadmaster-- and
there is some related question as to the manner of measurement, there is
no question that a problem existed concerning the hump and the runoff,
especially since the record shows that there were ties left swinging.
There is substantial evidence in the record to support the Carrier's
charges against Grievant.
-: :z ie
Award Number 20175 Page 2
In view of Grievant's life-time of service with the Carrier,
of some 44 years, demotion is not easy to bear, and it is contended
that this is excessive punishment. The Carrier points out, however,
that "this was the third incident in which he was guilty of making an
improper runoff, the first two of which resulted in derailment of a
train." In the light of the circumstances in this particular case,
the Board will not substitute its judgment for that of the Carrier.
FINDINGS: The Third Division of the Adjustment Board, upon the whole
record and all the evidence, finds and holds:
That the parties waived oral hearing;
That the Carrier and the Employes involved in this dispute
are respectively Carrier and Employes within the meaning of the Railway Labor Act, as approved June
That this Division of the Adjustment Board has jurisdiction
over the dispute involved herein; and
That the Agreement was not violated.
A W A R D
Claim denied.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Third Division
ATTEST
Executive Secretary
Dated at Chicago, Illinois, this 15th day of _(arch 1974.