NATIONAL RAILROAD ADJUSTMENT BOARD
THIRD DIVISION Docket Number MW-20812
Joseph A. Sickles, Referee
(Brotherhood of Maintenance of Way Employes
PARTIES TO DISPUTE:
(The Alton and Southern Railway Company
STATEMENT OF CLAIM: Claim of the System Committee of the Brotherhood that:
(1) The suspension of thirty days imposed upon Trackmen William
McHatten, Alvin Wren and Emmett Dinwiddie was without just and sufficient
cause and on the basis of unproven charges (System File K-1638-27).
(2) The charges against the above-named employes be stricken from
the record and payment be allowed to each of said employes for the monetary
loss each sustained, all in accordance with Rule 20A(d) of the agreement.
OPINION OF BOARD: Claimants were charged with "leaving your assignment
without authority about 12 Noon, Tuesday, September 19,
1972." Subsequent to investigation, each Claimant was assessed a thirty (30)
day suspension.
Claimants have urged certain procedural deficiencies in the handling
of this dispute. However, we are unable to find that those matters were raised,
for consideration on the property. They may not be raised here under that
circumstance.
It is conceded that none of the employees worked after noon on the
day in question, and the issue to be resolved is whether or not they reasonably
believed that they had the permission of the Foreman to be absent. The Organization argues that the
the stated intention of each Claimant to depart the premises - for good and
sufficient cause - and, at the very least, he tacitly acquiesced.
Carrier has cited numerous Awards in support of its contention that
this Board is not constituted to make determinations of credibility. Under the
authority of those Awards, we are required to accept the resolutions of credibility questions as mad
that the Foreman did not give specific permission to the employees to be absent
on the afternoon in question.
However, that determination does not resolve the dispute. It appears,
from a review of the Transcript of Investigation, that Carrier did not require
as formalized a granting of permission as was its right. For example, at Page
Award Number 20876 Page 2
Docket Number MW-20812
7 of the Transcript of Investigation, we note the employees " ..could have
come up to me and told me anything but they just left - one told me at 10:15
and he was sick and I said try to make it until 10:30."
When asked if it was part of his job to find out why a man goes home,
the Foreman replied:
"Some lay off on pay day and some say it none of my business."
Further, we have noted that a witness called by the Carrier stated,
when asked what the Foreman's general reply is when he is told that a person
is going home:
"He say OK. with a wave of the hand."
Surely, McHatten appeared to be suffering severely from the inordinate
heat of the day, and the Foreman's testimony indicates that it was completely
out of character for McHatten - categorized as a good worker and dependable -
to merely walk off of a job. From an entire review of the record, the Board
detects, as noted above, a very loose procedure concerning employees departing
their work station.
While it appears that the Foreman had advised his crew at about ten
(10) minutes before noon that the gang might have to do certain additional work
that could require them to "run late", he apparently did not make any inquiry
of the Claimants (ten (10) minutes later) when they said they were departing;
nor did he inquire as to the reason for their leaving the job. His testimony
in this regard, "No, I couldn't hold them" is susceptible to a number of interpretations.
While this Board does not condone employees departing their duty
assignment without permission, at the same time, we must consider the entire
record as it relates to whether or not they had reason to believe that their
departure was permissible under the circumstances. In this regard, we question
that the Foreman did not add to the situation by his inaction. Accordingly,
under this record, we feel that a ten (10) day suspension was sufficient.
Claimants shall be reimbursed for compensation lost beyond the period of the
ten (10) day suspension.
FINDINGS: The Third Division of the Adjustment Board, upon the whole record
and all the evidence, finds and holds:
That the parties waived oral hearing;
Award Number 20876 Page 3
Docket Number MW-20812
That the Carrier and the Employes involved in this dispute are
respectively Carrier and Employes within the meaning of the Railway Labor
Act,as approved June 21, 1934;
That this Division of the Adjustment Board has jurisdiction over
the dispute involved herein; and
That the Agreement was violated.
A W A R D
Claim sustained to the extent stated in the Opinion of the Board,
above.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Third Division
ATTEST;
a 00.
Executive ecretary
Dated at Chicago, Illinois, this 26th day of November 1975.