NATIONAL RAILROAD ADJUSTMENT BOARD
THIRD DIVISION Docket Number MW-22513
George S. Roukis, Referee
(Brotherhood of Maintenance of Way Employes
PARTIES TO DISPUTE:
(St. Louis-San Francisco Railway Company
STATEMENT OF CLAIM: "Claim of the System Committee of the Brotherhood
that:
(1) The dismissal of Track Foreman James H. Hollis on May 19,
1977 was without just or sufficient cause and on the basis of unproven
and disproven charges (System File B-940).
(2) The charge shall be stricken from the record and the
claimant shall be allowed payment for the assigned working hours
actually lost while out of service, all in conformance with Agreement
Rule 91(b)(6)."
OPINION OF BOARD: Claimant was suspended from service on May 19, 1977
immediately following a costly derailment in the
vicinity where he had recently engaged in a track surfacing assignment.
The Organization's General Chairman requested an investigative
hearing pursuant to Agreement procedures and claimant was afforded
this process on June 3, 1977.
The notice of investigation, dated May 25, 1977 stated that
the administrative inquiry would be directed toward developing the
facts in connection with his alleged violation of Rules 250, 255, 281,
419 and 425 of the Rules for the Maintenance of Way and Structures.
The hearing officer found him guilty of the charges and he
was permanently dismissed from service, effective June 7, 1977.
On July 7, 1977 Carrier informed the General Chairman that
while claimant was not solely responsible for the derailment he,
nevertheless, had "a certain amount of responsibility" in that he was
the foreman. It indicated, however, its amenability to returning
claimant to work effective July 11, 1977 but without pay for time lost,
which amounted to about sixty (60) days.
Award Number 225145 Page 2
Docket Number MW-22513
The efficacy and justification of this modified penalty has
been appealed to us for adjudicatory finality.
In reviewing the investigative transcript and reconstructing
the pattern of events preceding the derailment on may 18, 1977, we
find that claimant was not responsible for the derailment since the
record shows that the section of the track where it took place was
in a proper and safe condition when he finished his assignment the
previous day. The testimonial record is markedly consistent on
this point.
Sixteen trains had passed over that portion of the track
during the twenty-seven and one-half (27'x) hours period following
claimant's last inspection without incident or admonitory comment
from the crew members.
On the other hand, claimant's acknowledgment that he had
previously encountered problems with track kinking when working
welded rail south of the derailment site indicates that he should
have been more cautious. Its contiguous location warrants this
assessment. As foreman he should have recognized the possibility,
although perhaps remote, for a problem to develop. A greater level
of prudence was expected.
Because of this finding and our judgment that the sixty (60)
days de facto suspension is somewhat excessive when measured against
the degree of his incautious deportment, we will reduce the penalty
to ten (10) days suspension without pay.
FINDINGS; The Third Division of the Adjustment Board, upon the whole
record and all the evidence, finds and holds;
That the parties waived oral hearing;
That the Carrier and the Employes involved in this dispute
are respectively Carrier and Employes within the meaning of the
Railway Labor Act, as approved June 21, 1934;
That this Division of the Adjustment Board has jurisdiction
over the dispute involved herein; and
Award Number
22545
Page 3
Docket Number 1&1-22513
That the discipline was excessive.
A W A R D
Claim sustained in accordance with Opinion.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Third Division
ATTEST:
Executive Secretary
Dated at Chicago, Illinois, this 28th day of September
1979.