NATIONAL RAILROAD ADJUSTMENT BOARD
THIRD DIVISION Docket Number SG-22702
Martin F. Scheinman, Referee
(Brotherhood of Railroad Signalmen
PARTIES TO DISPUTE:
(Missouri Pacific Railroad Company
STATEMENT OF CLAIM: "Claim of the General Committee of the Brotherhood of
Railroad Signalmen on the Missouri Pacific Railroad
Company:
(a) Carrier violated the current Signalmen's Agreement, particularly
Rule 700, when it failed to prove charges brought against Signal Maintainer
M. F. Branz, Eads, Colorado, prior to and tried in an investigation held at
Eads August 4, 1977.
(b) Mr. Branz be paid for all time lost, including any overtime
earned by others on his assigned territory, beginning August 11, 1977 and
continuing until he is reinstated on his former position as Signal Maintainer
at Eads, Colorado. (Mr. Branz was dismissed from service under notice dated
August 10, 1977, _reinstated effective January 17, 1978, without pay for any
time lost)" jCarrier file: K 225-739/
OPINION OF BOARD: Claimant, Signal Maintainer M. F. Branz, after
investigation, was dismissed from service effective
August 10, 1977. Claimant was charged with (1) failing to comply with
instructions concerning the proper way to claim time on his time roll for
the July 4, 1977 Holiday, and (2) improper maintenance of the hot box
detector located at Mile Post 792, Pole 5, resulting in a failure of the
equipment to give proper indication. On a leniency basis, Claimant was
reinstated to service, effective January 18, 1978, but without pay for time
lost. In all, Claimant was out of service for a total of 137 work days.
We will first address the charge that Claimant failed to properly
maintain the hot box detector. The record contains numerous examples of
Claimant's failure to maintain the hot box detector. For example, Claimant
stated that he did not inspect the hot box detector during the intervening
week between July 8th and July 20th as required because he was "busy with
other things." He stated that he had failed to replace the hot box detector
tape even though he knew it needed to be changed. "I had planned to change
the tape before leaving on vacation but did not get back to the machine."
Award Number 22819 Page 2
Docket Number SG-22702
The record also discloses that he knew that the hot box detector
was located in a high dirt area. He was aware that the scanner needed to
be cleaned at least once a week. Yet, Claimant failed to take apart the
scanner and inspect the components. He admitted that the components had
not been cleaned from
July
8th until he left for vacation on
July
25th.
It was not until
July
26th, when the supervisor and foreman removed the
scanner covers and cleaned the mirror and lens that an inspection and
maintenance were actually performed.
Thus, the record conclusively establishes that Claimant was
negligent in his maintenance of the hot box detector. He is guilty of
failing to properly maintain it as charged.
The second charge is that Claimant failed to comply with
instructions concerning the proper way to claim time for
July 4,
1977.
The evidence indicates that Claimant had been told by Foreman Pipkin
that as a monthly employe, he was not to receive overtime for his work
on the
July
4th holiday. Nevertheless, Claimant improperly claimed
Class 3 time an his payroll record for the hours worked.
However, a close analysis of the record convinces this Board
that Claimant's entry for Class 3 time was not intended as a dishonest act.
While the entry was improper, he did not intend to defraud Carrier.
We are convinced that Claimant's improper entry was due to his
confusion aver Supervisor Brown's instructions (as related by Foreman Pipkin)
concerning the time worked. He honestly believed that putting the time
down was the appropriate way to handle his confusion. Claimant's uncertainty
was also due to the fact that he had previously occupied an hourly rated
position. There, time worked on a holiday is treated as overtime. While
Claimant should have followed the instructions, even if they were not
absolutely clear, and grieved later, we believe that Claimant's motive
must be considered in determining the appropriate penalty.
Given our finding that Claimant's entry for work on
July
4th was
an honest mistake and not a deliberate attempt to falsify his time roll,
we are of the opinion that Claimant's time out of service
wag
excessive.
A suspension of 90 days is appropriate for the proven offenses and we do
so find. Consistent with Article X of the November 16, 1971 Agreement
between the parties, Claimant shall be reimbursed for the period of his
unjust suspension.
Award Number 22819 Page 3
Docket Number
SG-22702
FINDINGS: The Third Division of the Adjustment Board, after giving the
parties to this dispute due notice of hearing thereon, and upon
the whole record and all the evidence, finds and holds:
That the Carrier and the Employes involved in this dispute are
respectively Carrier and Employes within the meaning of the Railway Labor
Act, as approved June 21, 1934;
That this Division of the Adjustment Board has jurisdiction over
the dispute involved herein; and
That the Agreement was violated.
A W A R D
Claim sustained in accordance with Opinion.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Third Division
ATTEST:
491AI.
Dated at Chicago, Illinois, this 18th day of April 1980.