(Brotherhood of Railroad Signalmen PARTIES TO DISPUTE:



STATEMENT OF CLAIM: "Claim of the General Committee of the Brotherhood of
Railroad Signalmen on the Missouri Pacific Railroad Company:

(a) Carrier violated the current Signalmen's Agreement, particularly Rule 700, when it failed to prove charges brought against Signal Maintainer M. F. Branz, Eads, Colorado, prior to and tried in an investigation held at Eads August 4, 1977.


earned by others on his assigned territory, beginning August 11, 1977 and
continuing until he is reinstated on his former position as Signal Maintainer
at Eads, Colorado. (Mr. Branz was dismissed from service under notice dated
August 10, 1977, _reinstated effective January 17, 1978, without pay for any
time lost)" jCarrier file: K 225-739/

OPINION OF BOARD: Claimant, Signal Maintainer M. F. Branz, after
investigation, was dismissed from service effective August 10, 1977. Claimant was charged with (1) failing to comply with instructions concerning the proper way to claim time on his time roll for the July 4, 1977 Holiday, and (2) improper maintenance of the hot box detector located at Mile Post 792, Pole 5, resulting in a failure of the equipment to give proper indication. On a leniency basis, Claimant was reinstated to service, effective January 18, 1978, but without pay for time lost. In all, Claimant was out of service for a total of 137 work days.

We will first address the charge that Claimant failed to properly maintain the hot box detector. The record contains numerous examples of Claimant's failure to maintain the hot box detector. For example, Claimant stated that he did not inspect the hot box detector during the intervening week between July 8th and July 20th as required because he was "busy with other things." He stated that he had failed to replace the hot box detector tape even though he knew it needed to be changed. "I had planned to change the tape before leaving on vacation but did not get back to the machine."



The record also discloses that he knew that the hot box detector was located in a high dirt area. He was aware that the scanner needed to be cleaned at least once a week. Yet, Claimant failed to take apart the scanner and inspect the components. He admitted that the components had not been cleaned from July 8th until he left for vacation on July 25th. It was not until July 26th, when the supervisor and foreman removed the scanner covers and cleaned the mirror and lens that an inspection and maintenance were actually performed.

Thus, the record conclusively establishes that Claimant was negligent in his maintenance of the hot box detector. He is guilty of failing to properly maintain it as charged.

The second charge is that Claimant failed to comply with instructions concerning the proper way to claim time for July 4, 1977. The evidence indicates that Claimant had been told by Foreman Pipkin that as a monthly employe, he was not to receive overtime for his work on the July 4th holiday. Nevertheless, Claimant improperly claimed Class 3 time an his payroll record for the hours worked.

However, a close analysis of the record convinces this Board that Claimant's entry for Class 3 time was not intended as a dishonest act. While the entry was improper, he did not intend to defraud Carrier.

We are convinced that Claimant's improper entry was due to his confusion aver Supervisor Brown's instructions (as related by Foreman Pipkin) concerning the time worked. He honestly believed that putting the time down was the appropriate way to handle his confusion. Claimant's uncertainty was also due to the fact that he had previously occupied an hourly rated position. There, time worked on a holiday is treated as overtime. While Claimant should have followed the instructions, even if they were not absolutely clear, and grieved later, we believe that Claimant's motive must be considered in determining the appropriate penalty.

Given our finding that Claimant's entry for work on July 4th was an honest mistake and not a deliberate attempt to falsify his time roll, we are of the opinion that Claimant's time out of service wag excessive. A suspension of 90 days is appropriate for the proven offenses and we do so find. Consistent with Article X of the November 16, 1971 Agreement between the parties, Claimant shall be reimbursed for the period of his unjust suspension.
                      Award Number 22819 Page 3

                      Docket Number SG-22702


FINDINGS: The Third Division of the Adjustment Board, after giving the
parties to this dispute due notice of hearing thereon, and upon
the whole record and all the evidence, finds and holds:

That the Carrier and the Employes involved in this dispute are respectively Carrier and Employes within the meaning of the Railway Labor Act, as approved June 21, 1934;

That this Division of the Adjustment Board has jurisdiction over the dispute involved herein; and

        That the Agreement was violated.


                      A W A R D


        Claim sustained in accordance with Opinion.


                            NATIONAL RAILROAD ADJUSTMENT BOARD

                            By Order of Third Division


ATTEST: 491AI.

        Executive Secretary


Dated at Chicago, Illinois, this 18th day of April 1980.