NATIONAL RAILROAD ADJUSTMENT BOARD
THIRD DIVISION Docket Number MST-23160
(Brotherhood of Maintenance of Way Employes
PARTIES TO DISPUTE:
(The Denver and Rio Grande Western Railroad Company
STATEMENT CF CLA114:. "Claim of the System Committee of the Brotherhood that:
(1) The dismissal of Track Patrolman D. J. Chess was Rithout
just and sufficUent cause and on the basis of unproven charges jSystem File
D-50-78/MW-26-7§j.
(2) Claimant D. J. Chess shall be afforded the remedy prescribed
in Rule 28(d)."
OPINION OF BOARD: Mr. D. J. Chess, the claimant, was a Track Patrolman
working between Cannon City and Salida on July 26, 1978.
Claimant in the performance of his duties operates a track motor car. The
record shows he passed all the qualifying examinations required by the
Carrier for a motor car operator. He also had the proper block authority
to operate in the territory involved. At approximately 2:45 P.M. on July 26,
1978, near Mile Post 180.6 the claimant was operating his motor car on a
one percent descending grade around a six degree curve on a heavily greased
rail when he saw Section Foreman Espinoza's motor car approaching from the
opposite direction ascending the grade about 80 feet away. Claimant Chess
testified that he was moving less than five miles per hour and his motor car
was nearly stopped at the point of contact. Claimant dismounted from the
motor car about 20 feet from contact. After contact claimant's motor car
was shoved back approximately 25 feet, indicating the speed and force of
the oncoming motor car.
Section Foreman Espinoza's motor car, carrying two other
employes, was pulling a push car loaded with three railroad ties,
a rail expander, rail fork, rail tongs, two big jacks, four shovels, three
picks, two spike maulers, two lining bars, a claw bar and a water can.
Section Foreman Espinoza's motor car was moving ten miles per hour or
faster at time of contact. Espinoza testified he was moving 10
MPH,
Section Laborer Rollison, one of the riders on Espinoza's car, estimated
the speed to be 15 MPH and Section Laborer Hugley, the other rider on his
car, estimated their speed to be 20 MPH.
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Docket Number MW-23160
Immediately prior to contact Espinoza and his two riders jumped
from the motor car. Espinoza and Hugley were injured, Espinoza wrenched
his knee and Hugley apparently had a more serious shoulder injury as he
testified he would be off work 3 or 4 weeks. Claimant Chess was not
injured. Extensive damage was done to both motor cars.
Formal investigation was held as scheduled on August 2, 1978.
A copy of the transcript of the investigation was made a part of the
record.
Both Section Foreman Espinoza and the claimant were dismissed
from service, the claimant by letter of August 8, 1978. The record shows
Espinoza acknowledging his part of the responsibility for the accident.
Claimant Chess denied any responsibility for the accident. Espinoza
requested and was granted reinstatement by the Carrier without back pay
on October 30, 1978. Six weeks later on December 11, 1978, Carrier
notified claimant he was reinstated as of that date. The claimant
rejected reinstatement.
Carrier's Safety Bale 405 of its Operating Department under
Track Car Operations reads:
"Track cars must be operated with the expectation of
finding the main track in use and care exercised to avoid
striking other track cars. It must be expected that on
Two or Mare Tracks, locomotives and trains may be operated
against the current of traffic without notice to track
car operators."
Rule 415 of the same Rules reads:
"Special care must be used when operating track cars
while rails are wet, icy or frosty and at all tftes
must be operated at a safe speed for existing conditions."
These apparently are the two Operating Rules the carrier contends claimant
violated.
The record is clear that claimant was operating his motor car
at a safe speed when he was engaging the six degree curve with heavily
greased rail, descending a one percent grade, at the time he first observed
the oncoming motor car. The record further shows his motor caf was moving
5 MPH or less at the time of impact. The oncoming heavily loaded motor
car, in accordance with the record, was moving between 10 and 20 MPH,
it too operating over the heavily greased rail. The Board is of the
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Docket Number MW-23160
opinion the only way the claimant could have avoided the accident would
have been to have removed his motor car from the track as it would have
been struck whether it was stopped or not. Claimant testified his car
was "nearly" stopped at the time of impact and this testimony was not
refuted. The record supports the position that claimant was exercising
every effort to comply with the rules, but conditions beyond his control
caused the accident.
The Board concludes, and so awards, that the claimant's service
record be cleared and he be reinstated with seniority and all other rights
unimpaired and with back pay from date held out of service until December 11,
1978, inclusive, when the Carrier offered reinstatement and claimant declined.
FINDIMS: The Third Division of the Adjustment Board, upon the whole record
and all the evidence, finds and holds:
That the parties waived oral hearing;
That the Carrier and the Employes involved in this dispute are
respectively Carrier and Employes within the meaning of the Railway Labor
Act, as approved June 21, 1934;
That this Division of the Adjustment Board has jurisdiction over
the dispute involved herein; and
That the Agreement was violated.
A W A R D
Claim sustained in accordance with the Opinion.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Third Division
ATTEST: /
Executive Secretary
Dated at Chicago, Illinois, this 12th day of September 1980.