- NATIONAL RA?LRDAD AWZJSUCENT HOARD
THIRD DIVISION Docket Number Mid-24030
Lamont E. Stallworth, Referee
(Brotherhood of Maintenance of Way Employes
PARTIES TO DISPUTE:
(Houston Belt, and Terminal Railway Company
STATIME.9T OF CLAIN: "Claim of the System Committee of the Brotherhood that:
(1) The dismissal of Trackman J. L. Lenton for 'failure to protect'
his
'assignment
about 3:30 p.m.., December.l9, 1979' vas without dust and sufficient cause and wholly disproportiona
(2) Trackman J. L. Lenton shall be reinstated with seniority,
vacation and all other rights unimpaired and he shall be compensated for all
wage loss suffered including holiday pay."
OPINION OF HOARD: The Claimant, J. L. Lentos was hired by the Carrier on
September 18, 1978 in its Maintenance of Way Department .
as
a
Track Laborer. 'Oa January 10., 1980 a formal. investigation was held into.
the matter that the 'Claimant on December 19, 1979 failed to protect his work
,assignment. Claimant was found guilty of leaving his assignment without per
mission sad was dismissed from service. In conference on -September 12, 1980,
Carrier's Director of Labor Relations offered reinstatement on a leniency basis,
without pay, to Trackman Lenton and Trachea IaVeigae, also involved is same
incident. Claimant Lenton refused the offer.
The Carrier maintains that on December 19, 1979 Trackman Lenton left
his assignment without permission even though he knew that as emergency existed
due to a broken rail. Claimant knew and had observed the proper "mark off" procedures, but in the in
merely walked
off from his fob without permission or notifying Foreman Hunt. Testimony by Foreman Hunt states that
of the men on his gang heard him say that they were going to work overtime and
that Trachea Lenton did not ask permission to be off. Foreman Hunt further
testified that Trackmaa Lenton had always performed overtime in the past when
he was requested unless Claimant had permission to get off.
The Claimant maintains that he was not required nor asked by Foremen
Hunt to perform overtime services. Testimony by Lenton states that he informed
Foreman Hunt that he vas not able to work overtime because he did not have a
ride home. Since Foreman Hunt made it clear that he did not care if Claimant
worked as not sad had instructed Claimant to talk to Supervisor Blakley, Claimant felt that he was g
Claimant testified that had he been instructed to remain at the work site and
informed as to the urgency of the work.. he would not have left. Further Claimant testified that he
Foreman Hunt fully understood that Claimant was leaving the property.
_ Award Number 23978 Page 2
Docket Number MW-24030
Upon careful consideration of th~.,record herein the Board concludes
that dismissal in this case is excessive. (There is substantial evidence is
the record which supports the conclusion that Claimant dial not have a full
understanding that he was being ordered to work overtime. The Board further,
notes the Claimant's heretofore unblemished work record and the fact that
Claimant testified that if he had understood that he was being ordered to work
overtimes he would have complied with this order. Accordingly we hold that
Claimant shall be reinstated without backpay and with seniority and all other
rights unimpaired.
FIL'm>T1G3: The Tn1.xd. Division of the Adjustment Boards . upon the. whole rec
and all the evideacej, finds and holds:
That the parties waived oral hearing;
That the Carrier sad the Employes involved in this dispute are
respectively Carrier and Employee within the meaning of the Railway Labor
Acts as approved June 21, 1934;
That this Division of the Adjustment Board has jurisdiction
over the dispute involved herein; and
That the discipline vas excessive.
A W A R D . .
Clsim.sustaiaed in accordance with the opinion.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Third Division
ATTEST: Acting Executive Secretary
National Railroad Adjustment Board
;.
By
Rosemarie Breach - Administrative Assistant
,,\~\ ~.,,
_ _ .
c` ~
Dated at Chicago, Illinois, this 27th day of August 1982. \ --____--