NATIONAL RAILROAD ADJUSTMENT BOARD
THIRD DIVISION Docket Number MW-24101
Herbert L, Marx, Jr., Referee.
(Brotherhood of Maintenance of Way Employes
PARTIES TO DISPUTE: (
(Detroit, Toledo and Ironton Railroad Company
STATEMENT OF CLAIM: "Claim of the System Committee of the Brotherhood that:
(1) The thirty day suspension (5 days actual and 25 days record)
imposed upon Section Foreman Hobert Sack for alleged failure to properly line
'the south switch of Thackery Siding' on February 5,
1979
was unwarranted, on
the basis of unproven charges and in violation of the Agreement.
(2) Section Foreman Hobert Back shall now be allowed the benefits
prescribed in Agreement Rule
34(e).
OPINION OF BOARD: Claimant is a Section Foremen who was directed, with two
crew members, to perform switch-cleaning duties involving
snow removal. He was charged with failure to realign a switch which resulted in
a train "encountering and running through an improperly lined main track switch"
and was subject to an investigative hearing. Cited in the Carrier's investigation
notice were Rule "N" and Rules
866
and
869.
In particular, Rule
869
reads is pertinent part that Maintenance of
Way Foremen "must personally attend and supervise the opening and closing of
switches."
The Organization argues that the Claimant was not subject to a fair
and proper investigative hearing, since one Carrier representative issued the
notice of the hearing, conducted the hearing, reviewed the results, and determined
the disciplinary penalty. While there are instances in which a hearing officer's
multiple role may well interfere with his impartial conduct of the hearing, the
Board does not find this to be the case here. The hearing officer. was in no
way connected with the incident itself; the Claimant and the Organization were
not impaired in their presentation in any way; and the determination of penalty
after a hearing by the hearing officer is not prohibited by rule.
The record shows that the Claimant and his crew members were directly
involved with cleaning the switch dust prior to its being overrun by a train.
The Carrier had proper grounds for holding that the Claimant was responsible
for failing to determine that the switch was properly set after the cleaning had
been completed. This failure could have led to serious consequences and did in
actuality result in train delay and switch damage.
The thirty-day suspension (of which only five days was ail actual
suspension) was not inappropriate.
Award Number 24080 Page 2
Docket Number Pb1-24101
FINDINGS: The Third Division of the Adjustment Board, upon the whole record
and all the evidence, finds and holds:
That the parties waived oral hearing;
That the Carrier and the Employee involved in this dispute are
respectively Carrier and Employee within the meaning of the Railway Labor Act,
as approved June 21,
193+;
That this Division of the Adjustment Board has jurisdiction aver
the dispute involved herein; and
That the Agreement was not violated.
A W A R D
Claim denied.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Third Division
Attest: Acting Executive Secretary
National Railroad Adjustment Board
B
d:t.
y
Rosemarie Brasch - Administrative Assistant
Dated at Chicago,
Illinois,
this 5th day of January
1983.
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