NATIONAL RAILROAD ADJUSTMENT BOARD
THIRD DIVISION Docket Number
MW-24173
(Brotherhood of Maintenance of Way Employes
PARTIES TO DISPUTE:
Bangor and Aroostook Railroad Company
STATEMENT OF CIAIM: "Claim of the System Committee of the Brotherhood that:
(1) The dismissal of Sub-Foreman Charles H. Boss, Jr. for alleged
'Failure to perform your duties as Sub-Foreman in a responsible manner' and for
alleged violation of Rules '110',
'275',
'A',
'284', '290'
and
'4118'
was without
just and sufficient cause, unwarranted, on the basis of unproven charges and in
violation of the Agreement (Carrier's File
149.4.3).
(2) Sub-Foreman Charles H. Boss, Jr. shall now be allowed the benefits
prescribed in Section 1(c) of Article IV.
OPINION OF BOARD: Claimant, a Sub-Foreman on the tie gang, was dismissed from
service following an investigation held on August
14
and
14,
1980.
The Carrier had charged Claimant with a number of different offenses.
Though the
Organization contended the notice of charges was imprecise, we find
that the notice dated August
7, 1980
apprised Claimant and his representative
with sufficient details concerning the alleged infractions.
At the investigation, several trackmen on the tie gang related that on
August
5, 1980,
Claimant drove a motor car (at high speed) toward them without
warning while they were working inside the track. They stepped out of the way
just before the motor car passed. The Assistant Superintendent of Track and a
Machine Operator testified that Claimant improperly dumped untreated sewage
from the outfit's living cars into a ditch along the right of way on June
30,
1980.
The Carrier also presented evidence indicating Claimant was partially
responsible for damage to a personnel trailer which collided with a train. An
examination of the trailer after the accident disclosed that the trailer had not
been properly secured and that Claimant had not placed a derail on the track.
Other testimony at the investigation related to Claimant's harrassment of a
deputy sheriff, his failure to timely file a personal
injury
report, and his
alleged hostile relationship with some of the members of the tie gang.
When the Carrier decided upon the measure of discipline to impose on
Claimant, the Carrier not only reviewed Claimant's prior record but also relied
on a June
8, 1972
letter of Understanding between the Carrier and Claimant. In
essence, the
1972
Letter (which
had resolved a prior disciplinary matter) stated
that Claimant could be discharged if he committed any subsequent rule infraction.
Characterizing the Carrier's evidence as gossip, unsubstantiated gripes,
and personality conflicts, the Organization contends that there is no credible
evidence in the record showing Claimant engaged in any misconduct. In addition,
the Organization challenges the Carrier's reliance on the
1972
Letter of
Award Number 24278 Page 2
Docket Number M-24173
Understanding to justify Claimant's dismissal. According to the Organization,
the Carrier's failure to raise the terms of the 1972 letter for eight years was
an unreasonable delay which prejudiced Claimant. Citing the doctrine of laches,
the organization argues that the Carrier is barred from using the 1972 letter
against Claimant. The Carrier, on the other hand, submits that there is overwhelming evidence demons
and irresponsible fashion. When Claimant's poor prior discipline record is taken
into account in conjunction with the 1972 letter, the Carrier contends that
dismissal was the appropriate measure of discipline.
After carefully reviewing the lengthy record in this case, we conclude
that the Carrier presented substantial evidence proving that Claimant committed
not just one infraction but several offenses during the summer of 1980.
On August 5, 1980, Claimant recklessly operated a motor car which
could have resulted in serious injury to the trackman. Perhaps Claimant was
merely trying to scare his gang. However, his actions were dangerous and went
far beyond 'the usual interaction found in track gangs. Furthermore, Claimant
improperly disposed of untreated sewage, caused damage to a personnel trailer
by not observing safety precautions and harassed a peace officer. Claimant has
demonstrated, by his own conduct, that he is unable to responsibly carry out
his duties.
Given Claimant's poor prior record, we do not find any justification
for reducing the assessed disciplix. This Board does not need to address the
parties arguments regarding the effect of the 1972 Letter of Understanding.
Standing alone, the severity of Claimant's offenses as well as his poor past
record constitute an independent basis for upholding the dismissal.
FINDINGS: The Third Division of the Adjustment Board, upon the whole record and
all the evidence, finds and holds:
That the parties waived oral hearing;
That the Carrier and the Employes involved in this dispute are
respectively Carrier and Employes within the meaning of the Railway Labor Act,
as approved June 21,
1934;
That this Division of the Adjustment Board has jurisdiction over the
dispute involved herein; and
That the Agreement was not violated.
A W A R D
Claim denied.
Award Number
24278
Docket Number
MW-24173
Page
3
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Third Division
Attest: Acting Executive Secretary
National Railroad Adjustment Board
Rosemarie Brasch - Administrative Assistant
Dated at Chicago, Illinois, this
31st day of March 1983.