NATIONAL RAILROAD ADJUSTMENT BOARD
THIRD DIVISION Locket Number SG-24151
John B. LaRocco, Referee
(Brotherhood of Railroad Signalmen
PARTIES TO DISPUTE:
(Southern Railway Company
STATEMENT OF CLAIM: Claim of the General Committee of the Brotherhood of
Railroad Signalmen on the Southern Railway System et a1:
Claim on behalf of the following signal employees who were dismissed
from service as a result of an investigation held on February 6, 1980, with a
request that they be reinstated with seniority rights unimpaired and paid for
all time lost.
Claim No. 1, Foreman Robert Carroll - General Chairman file:
SG-153 Carrier file: SG-432.
Claim No. 2, Lead Signalman T. L. Davis - General Chairman file:
SG-154 Carrier file: SG-431.
Claim No.3. Signalman Robert Johnson, Jr., General Chairman file:
SR-158 Carrier file: SG-434
Claim No. 4. Assistant Signalman A. W. Bustos - General Chairman file:
SR-156 Carrier file: SG-433.
OPINION OF BOARD: This case is the consolidated appeal of the dismissals of
four members of a signal gang following an investigation
involving all four Claimants held on February 6, 1980. By notice dated January 30,
1980, each Claimant was given written notification of the charges placed against
him. in summary, Claimant Carroll, the Signal Foreman, was charged with
failing to properly supervise the gang. The Lead Signalman, Claimant Davis,
was accused of tampering with evidence and conduct unbecoming an employee.
Claimants Johnson and Bustos, a Signalman and Assistant Signalman respectively, were
charged with failure to properly and competently carry out their duties.
To fully understand this case, we must relate the facts in some detail.
January 25, 1980, the gang was assigned to install circuit controllers on the
Illinois Grain siding at Browns, Illinois. When the gang arrived at the work
site, Claimant Carroll observed that the centering device was detached from
the siding switch. He brought this defect to the attention of several gang
members and evidently Claimant Bustos began to repair the centering device.
To ease the tension on the device, Claimant Bustos unlocked the switch (which
was properly aligned for mainline movement) and opened it halfway. When
Claimant Carroll noticed Claimant Bustos cvrking on the switch, the Foreman
took him off that job and directed Claimant Johnson to finish the work. Claimant
Johnson complied, However, after completing the repair, Claimant Johnson left
the switch in an open position (for movement from the mainline into the siding).
Award Number 24766
Docket Number SG-24151 Page 2
Moments later, eastbound Train No. 127 came down the mainline at
approximately forty-five miles per hour. Immediately before reaching the switch,
Engineer Marshall saw a red target and he quickly confirmed that the switch
points were lined for movement into the siding. He warned his brakeman and put
the train in emergency. The train started into the siding and three engines
and twenty-five cars derailed. Several crew members, including Engineer Marshall,
were injured. Fortunately, the signal gang members were able to run clear of
the oncoming train and, thus, were uninjured. Superintendent mills testified
that due to the derailment, the carrier incurred almost a million dollars of
damage to Carrier equipment and shippers' lading.
When Company officials arrived at the scene of the wreck, they promptly
ascertained that the switch was locked and lined for the mainline. When they
interviewed Claimants, none of them informed the Carrier that they had worked
on the switch just prior to the derailment. Late in the evening of January 26,
1980, Claimants recanted and frankly admitted that they had worked on the switch
and inadvertently left it in an open position. Despite these admissions, they
all disavowed any direct responsibility for causing the derailment. In addition,
Claimant Davis conceded that after the derailment, he saw the switch was lined
for the mainline with the lock lying on a nearby tie. He then locked the switch.
When he was first questioned by carrier officials, he failed to disclose that
he locked the switch after the accident. He did so to avoid embarrassing other
members of the gang because he mistakenly believed the switch had not been a
factor in the derailment. A11 Carrier officials investigating the derailment
had been puzzled and confused since they observed the switch securely locked
and properly lined for mainline movement though the position of the engines
suggested that the train had started to turn into the siding. The Western
Division Superintendent had concluded that if Train No. 127 entered the open
switch at a high rate of speed, the enormous pressure would push the switch
points back to normal mainline alignment. However, until Claimant Davis revealed
that he put the lock on subsequent to the derailment, the officers were unable
to pinpoint the exact cause of the derailment.
Initially, the Organization contends that the Carrier unjustifiably
withheld Claimants from service pending the February 6, 1980 investigation.
disagree. In Third Division Award No. 15828 (Ives), involving these same parties,
the Board rules that the Carrier could reasonably exercise its discretion to
withold a charged employee from service pursuant to the express language of
Rule 23. The transcript of the investigation shows that all four Claimants
were given ample opportunity to present all defenses, to explain their actions
and to cross-examine the Carrier's witnesses. Indeed, there is little dispute
regarding the essential facts. Thus, Claimants received a fair Rule 23 hearing.
To ascertain if each Claimant committed the charged offense, we must
evaluate the record to determine if the Carrier presented substantial evidence
to prove the charges leveled against each Claimant. At the onset, we note that
the derailment was caused by the open siding switch at Illinois Grain. Therefore,
we must decide, on an individual basis, if each Claimant was responsible for
the improperly aligned switch.
Docket Number SG-24151 Page 3
Claimant Davis held no responsiblity for the position of switch prior
to the derailment but he deliberately tampered with the switch lock immediately
after the wreck occurred. His foolhardy conduct concealed the true cause of
the derailment. Claimant Davis locked the switch with the specific
intent of
protecting his fellow gang members. Though he later admitted his misconduct,
he had, for a time, effectively thwarted the Carrier's ability to investigate
the derailment. Thus, he intentionally tampered with evidence having a direct
bearing on the derailment.
Claimant Bustos initially opened the switch. Though he apparently
did so with his Foreman's permission, he should have informed Claimant Johnson
that the switch was open when Johnson later took over the repair task. Also,
Claimant Bustos should not have moved the switch without first complying with
the applicable operating rules for safeguarding mainline movement.
Claimant Johnson, who worked on the switch after Claimant Bustos, did
not realize that Claimant Bustos had unlocked and opened the switch. Inexplicably,
Claimant Johnson finished the necessary repairs but then left the switch without
realigning it for the mainline. However, for several reasons, he recklessly
performed his duties. First, he worked within eight feet of the open switch
points and so he should have noticed their position. Second, he should have
known that Claimant Bustos would have to open the switch to attach the centering
device. Third, he walked away from the switch without checking its position.
A fundamental part of his job was to make certain (after completing his work)
that the switch was safe for mainline train movement. Since he had relieved a
fellow worker, Claimant Johnson should have been especially alert for any errors
made by Claimant Bustos. Claimant Johnson cannot shift the blame for his
negligence to other workers merely because they were also responsible for the
unsafe condition of the switch. Fourth Division Award No. 3425 (Eischen).
Claimant Carroll was responsible for the cork performed by employees
under his command. Claimant Carroll imprudently permitted his workers to open
the switch. His gang was not even assigned to perform any repairs on the switch.
Once he allowed Claimant Bustos to open the switch, he should have closely
supervised his work since the switch repair was far more crucial than
installing the controllers on the siding. Claimant Carroll suddenly removed
one worker from the switch and substituted another. This lack of continuity
without supervision indirectly caused both workers to leave the switch open and
unattended. Finally, like the other Claimants, Claimant Carroll impeded the
carrier's inquiry into causes of the accident by withholding pertinent
information and denying that the gang had worked on the switch.
We, therefore, find that though no one Claimant was solely at fault,
all four Claimants were jointly responsible for the improper position of the
switch. The final issue is whether or not dismissal was the appropriate penalty.
Claimants Carroll and Johnson committed such gross negligence that we cannot
find any justification for reducing their discipline. The former held ultimate
responsibility and the latter had numerous chances to place the switch in its
correct position. Similarily, Claimant Davis,
intentional attempt
to undermine
the Carrier's investigation constitutes deceit and disloyalty. We must uphold
his discharge. There is, however a mitigating circumstance which demonstrates that
the discipline assessed against Claimant Bustos was excessive and unduly harsh.
Award Number 24766
Docket Number SG-24151 Page 4
Though Claimant Bustos should have informed Claimant Johnson that the switch
was open, he was quickly removed from the job by his Foreman. Claimant Bustos
was obligated to comply with his foreman's directive. Thus, Claimant Bustos
was less culpable than the other Claimants. Claimant Bustos should be
reinstated to service, with his seniority unimpaired but without compensation
for time lost.
FINDINGS: The Third Division of the Adjustment Board, after giving the parties
to this dispute due notice of hearing thereon, and upon the whole
record and all the evidence, finds and holds:
That the Carrier and the Employes involved in this dispute are
respectively Carrier and Dnployes within the meaning of the Railway Labor Act,
as approved June 21, 1934;
That this Division of the Adjustment Board has jurisdiction over
the dispute involved herein; and
That the Discipline was excessive as to Claimant Bustos only.
A W A R D
1. Claims of Carroll, Johnson and Davis are denied.
2. Claim of Bustos is sustained in accordance with the Opinion.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Third Division
ATTEST- r~
Nancy ver - Executive Secretary
Dated at Chicago, Illinois, this 13th day of April, 1984