PARTIES TO DISPUTE:


STATEMENT OF CLAIM: Claim of the General Committee of the Brotherhood of


Claim on behalf of the following signal employees who were dismissed from service as a result of an investigation held on February 6, 1980, with a request that they be reinstated with seniority rights unimpaired and paid for all time lost.

Claim No. 1, Foreman Robert Carroll - General Chairman file: SG-153 Carrier file: SG-432.

Claim No. 2, Lead Signalman T. L. Davis - General Chairman file: SG-154 Carrier file: SG-431.

Claim No.3. Signalman Robert Johnson, Jr., General Chairman file: SR-158 Carrier file: SG-434

Claim No. 4. Assistant Signalman A. W. Bustos - General Chairman file: SR-156 Carrier file: SG-433.

OPINION OF BOARD: This case is the consolidated appeal of the dismissals of
four members of a signal gang following an investigation
involving all four Claimants held on February 6, 1980. By notice dated January 30,
1980, each Claimant was given written notification of the charges placed against
him. in summary, Claimant Carroll, the Signal Foreman, was charged with
failing to properly supervise the gang. The Lead Signalman, Claimant Davis,
was accused of tampering with evidence and conduct unbecoming an employee.
Claimants Johnson and Bustos, a Signalman and Assistant Signalman respectively, were
charged with failure to properly and competently carry out their duties.

To fully understand this case, we must relate the facts in some detail. January 25, 1980, the gang was assigned to install circuit controllers on the Illinois Grain siding at Browns, Illinois. When the gang arrived at the work site, Claimant Carroll observed that the centering device was detached from the siding switch. He brought this defect to the attention of several gang members and evidently Claimant Bustos began to repair the centering device. To ease the tension on the device, Claimant Bustos unlocked the switch (which was properly aligned for mainline movement) and opened it halfway. When Claimant Carroll noticed Claimant Bustos cvrking on the switch, the Foreman took him off that job and directed Claimant Johnson to finish the work. Claimant Johnson complied, However, after completing the repair, Claimant Johnson left the switch in an open position (for movement from the mainline into the siding).



Moments later, eastbound Train No. 127 came down the mainline at approximately forty-five miles per hour. Immediately before reaching the switch, Engineer Marshall saw a red target and he quickly confirmed that the switch points were lined for movement into the siding. He warned his brakeman and put the train in emergency. The train started into the siding and three engines and twenty-five cars derailed. Several crew members, including Engineer Marshall, were injured. Fortunately, the signal gang members were able to run clear of the oncoming train and, thus, were uninjured. Superintendent mills testified that due to the derailment, the carrier incurred almost a million dollars of damage to Carrier equipment and shippers' lading.

When Company officials arrived at the scene of the wreck, they promptly ascertained that the switch was locked and lined for the mainline. When they interviewed Claimants, none of them informed the Carrier that they had worked on the switch just prior to the derailment. Late in the evening of January 26, 1980, Claimants recanted and frankly admitted that they had worked on the switch and inadvertently left it in an open position. Despite these admissions, they all disavowed any direct responsibility for causing the derailment. In addition, Claimant Davis conceded that after the derailment, he saw the switch was lined for the mainline with the lock lying on a nearby tie. He then locked the switch. When he was first questioned by carrier officials, he failed to disclose that he locked the switch after the accident. He did so to avoid embarrassing other members of the gang because he mistakenly believed the switch had not been a factor in the derailment. A11 Carrier officials investigating the derailment had been puzzled and confused since they observed the switch securely locked and properly lined for mainline movement though the position of the engines suggested that the train had started to turn into the siding. The Western Division Superintendent had concluded that if Train No. 127 entered the open switch at a high rate of speed, the enormous pressure would push the switch points back to normal mainline alignment. However, until Claimant Davis revealed that he put the lock on subsequent to the derailment, the officers were unable to pinpoint the exact cause of the derailment.

Initially, the Organization contends that the Carrier unjustifiably withheld Claimants from service pending the February 6, 1980 investigation. disagree. In Third Division Award No. 15828 (Ives), involving these same parties, the Board rules that the Carrier could reasonably exercise its discretion to withold a charged employee from service pursuant to the express language of Rule 23. The transcript of the investigation shows that all four Claimants were given ample opportunity to present all defenses, to explain their actions and to cross-examine the Carrier's witnesses. Indeed, there is little dispute regarding the essential facts. Thus, Claimants received a fair Rule 23 hearing.

To ascertain if each Claimant committed the charged offense, we must evaluate the record to determine if the Carrier presented substantial evidence to prove the charges leveled against each Claimant. At the onset, we note that the derailment was caused by the open siding switch at Illinois Grain. Therefore, we must decide, on an individual basis, if each Claimant was responsible for the improperly aligned switch.
          Award Number 24766

                    Docket Number SG-24151 Page 3


Claimant Davis held no responsiblity for the position of switch prior to the derailment but he deliberately tampered with the switch lock immediately after the wreck occurred. His foolhardy conduct concealed the true cause of the derailment. Claimant Davis locked the switch with the specific intent of protecting his fellow gang members. Though he later admitted his misconduct, he had, for a time, effectively thwarted the Carrier's ability to investigate the derailment. Thus, he intentionally tampered with evidence having a direct bearing on the derailment.

Claimant Bustos initially opened the switch. Though he apparently did so with his Foreman's permission, he should have informed Claimant Johnson that the switch was open when Johnson later took over the repair task. Also, Claimant Bustos should not have moved the switch without first complying with the applicable operating rules for safeguarding mainline movement.

Claimant Johnson, who worked on the switch after Claimant Bustos, did not realize that Claimant Bustos had unlocked and opened the switch. Inexplicably, Claimant Johnson finished the necessary repairs but then left the switch without realigning it for the mainline. However, for several reasons, he recklessly performed his duties. First, he worked within eight feet of the open switch points and so he should have noticed their position. Second, he should have known that Claimant Bustos would have to open the switch to attach the centering device. Third, he walked away from the switch without checking its position. A fundamental part of his job was to make certain (after completing his work) that the switch was safe for mainline train movement. Since he had relieved a fellow worker, Claimant Johnson should have been especially alert for any errors made by Claimant Bustos. Claimant Johnson cannot shift the blame for his negligence to other workers merely because they were also responsible for the unsafe condition of the switch. Fourth Division Award No. 3425 (Eischen).

Claimant Carroll was responsible for the cork performed by employees under his command. Claimant Carroll imprudently permitted his workers to open the switch. His gang was not even assigned to perform any repairs on the switch. Once he allowed Claimant Bustos to open the switch, he should have closely supervised his work since the switch repair was far more crucial than installing the controllers on the siding. Claimant Carroll suddenly removed one worker from the switch and substituted another. This lack of continuity without supervision indirectly caused both workers to leave the switch open and unattended. Finally, like the other Claimants, Claimant Carroll impeded the carrier's inquiry into causes of the accident by withholding pertinent information and denying that the gang had worked on the switch.

We, therefore, find that though no one Claimant was solely at fault, all four Claimants were jointly responsible for the improper position of the switch. The final issue is whether or not dismissal was the appropriate penalty. Claimants Carroll and Johnson committed such gross negligence that we cannot find any justification for reducing their discipline. The former held ultimate responsibility and the latter had numerous chances to place the switch in its correct position. Similarily, Claimant Davis, intentional attempt to undermine the Carrier's investigation constitutes deceit and disloyalty. We must uphold his discharge. There is, however a mitigating circumstance which demonstrates that the discipline assessed against Claimant Bustos was excessive and unduly harsh.
                    Award Number 24766

                    Docket Number SG-24151 Page 4


Though Claimant Bustos should have informed Claimant Johnson that the switch was open, he was quickly removed from the job by his Foreman. Claimant Bustos was obligated to comply with his foreman's directive. Thus, Claimant Bustos was less culpable than the other Claimants. Claimant Bustos should be reinstated to service, with his seniority unimpaired but without compensation for time lost.

FINDINGS: The Third Division of the Adjustment Board, after giving the parties
to this dispute due notice of hearing thereon, and upon the whole
record and all the evidence, finds and holds:

That the Carrier and the Employes involved in this dispute are respectively Carrier and Dnployes within the meaning of the Railway Labor Act, as approved June 21, 1934;

That this Division of the Adjustment Board has jurisdiction over the dispute involved herein; and

        That the Discipline was excessive as to Claimant Bustos only.


                        A W A R D


        1. Claims of Carroll, Johnson and Davis are denied.


        2. Claim of Bustos is sustained in accordance with the Opinion.


                            NATIONAL RAILROAD ADJUSTMENT BOARD By Order of Third Division


ATTEST- r~
Nancy ver - Executive Secretary

        Dated at Chicago, Illinois, this 13th day of April, 1984