NATIONAL RAILROAD ADJUSTMENT BOARD
THIRD DIVISION Locket Number SG-24178
John B. LaRocco, Referee
(Brotherhood of Railroad Signalmen
PARTIES TO DISPUTE:
(Western Pacific Railroad Company
STATEMENT OF CLAIM: Claim of the General Committee of the Brotherhood of
Railroad Signalmen on the Western Pacific Railroad Company:
On behalf of F. J. Falsetti, who was dismissed by letter dated June
18, 1980, for reinstatement to his former position of TCS Maintainer, 2bbin,
California, compensation for all time lost, and that his record be cleared of any
and all notations related to the cause of his dismissal.
[Carrier file: GM Case No. 12534-1980-BRS LC No. BRS-40 En g. Dept.]
OPINION OF BOARD: The basic facts in this case are in dispute. According to
the Carrier's Signal Test Foreman, Claimant, a signal maintainer,
asked the Foreman to help him locate the source of a signal malfunction at
Virgilia on May 23, 1980. The Foreman also testified that Claimant admitted
that he had placed jumper cables directly from the right track battery
to the terminal board when he could not ascertain the cause of the problem
the day before. Since the jumper cables bypassed the track signal wire, the
signal on the dispatcher's console would continuously register clear regardless
of the presence of either a train or broken rail on the Virgilia siding. The
Foreman removed the jumper cables and the detector relay fell to erase the clear
signal. After a short inspection, the Test Foreman discovered a broken track
wire buried in the ballast. He repaired the wire which cured the signal problem.
A Maintenance of Way Foreman observed the Test Foreman locate and repair the
broken signal wire. There was no evidence that the wire had been previously
spliced because it was buried deep in the ballast.
Claimant specifically denies any responsibility for the jumper cables.
On the contrary, he testified that when signal trouble occurred at Virgilia on
the evening of May 22, 1980, he repaired the damaged wire and left the signal
system in working order. He did acknowledge that when he accompanied the Test
Foreman to Virgilia the next day, jumper cables connected the battery and terminal
board.
Subsequent to an investigation held on June 11, 1980, the Carrier
dismissed Claimant from service.
The organization argues that the Carrier held an untimely investigation
and therefore, this Board should summarily sustain the claim. The Carrier sent
written notice to Claimant informing him that a formal investigation would be
held on June 5, 1980. The hearing was postponed to June 11, 1980 at the Local
Chairman's request. Rule 68 mandates that the Carrier convene the investigation
within ten calendar days of either the date the alleged offense occurred or the
date management first learned the alleged offense occurred. On the property,
the Carrier contended it did not know Claimant had committed any offense until
June 2, 1980. However, at the investigation, the Test Foreman clearly stated
that he notified the Signal Supervisor of Claimant's alleged misconduct on May 27,
1980. Though the Test Foreman did not promptly notify his supervisor of the
Award Number 24768
Docket Number SG-24178 Page 2
incident, an intervening holiday weekend probably contributed to the delay in
informing management. Since the investigation was originally scheduled within
ten calendar days of May 27, 1980, the Carrier met the Rule 68 time constraints.
On the merits, the evidence is substantial, almost overwhelming that
Claimant left the signal system at Virgilia in an unsafe and inoperable condition
on the evening of May 22, 1980. Despite Claimant's blanket denials, the other
evidence in the record conclusively demonstrates that he was responsible for
the jumper cables. First, the Test Foreman would not have been at Virgilia but
for Claimant's request. Claimant surely would not have asked the Foreman to go
to Virgilia unless there was still a problem with the signal system. Thus, the
hearing officer could discount Claimant's contention that he completely repaired
the problem the night before. Second, a reliable witness observed the Test
Foreman pull the broken signal wire out of the ballast. Third, Claimant offered
no explanation for the jumper cables. He was the last person at the site the
previous day and the first person (with the Test Foreman) to enter the signal
facility on May 23, 1980.
The Organization also argues that the discipline was excessive and
unduly harsh. While Claimant had been employed by the Carrier for only two
years, we agree. He did voluntarily bring the problem to the Test Foreman's
attention. Claimant shall be reinstated to service, with his seniority unimpaired
but without compensation for time lost. However, Claimant should understand
that he must strictly comply with all rules. We expect Claimant to competently
and conscientiously perform his duties upon his return to service.
FINDIAGS: The Third Division of the Adjustment Board, ,upon the whole record
and all the evidence, finds and holds:
That the parties waived oral hearing;
That the Carrier and the Employes involved in this dispute are respectively
Carrier and FSnployes within the meaning of the Railway Labor Act, as approved
June 21, 1934;
That this Division of the Adjustment Board has jurisdiction over the
dispute involved herein; and
That the discipline was excessive.
A W A R D
Claim sustained in accordance with the Opinion.
NATIONAL RAILROAD ALi7USTh1ENT BOARD
By Order of Third Division
Attest · 'Nancy . Aver - Executive Secretary
Dated at Chicago, Illinois this 13th day of April, 1984