NATIONAL RAILROAD ADJUSTMENT BOARD
THIRD DIVISION Docket Number MW-24982
Hyman Cohen, Referee
(Brotherhood of Maintenance of Way Employes
PARTIES TO DISPUTE:
(Colorado and Southern Railway Company
STATEMENT OF CLAIM: "Claim of the System Committee of the Brotherhood that:
(1) The disciplinary demotion of Foreman D. W. Bowser as section
foreman was without just and proper cause and was an abuse of justice and
discretion by the Carrier (System File C-35-81 /G-90 MW).
(2) Mr. D. W. Bowser's seniority as section foreman be restored and
unimpaired and he shall be allowed the difference betweeen what he would have
received at the section foreman's rate and what he was paid at the section
laborer's rate until he is returned to work as a section foreman with seniority
as such unimpaired."
OPINION OF BOARD: As a result of an investigation which was held on August 31,
1981, the Claimant was demoted from the position of foreman
to laborer because he was found responsible for the improper track conditions
resulting in the derailment of Train 142 at Boulder, Colorado on August 21,
1981.
On August 21, 1981, the Claimant was in charge of a two-man crew that
was engaged in replacing head blocks (ties). The record discloses that in
replacing the head blocks ties, the Claimant was derelict in not replacing the
switch point protector back on the switch point to provide full support and to
brace the stock rail. This allowed the s·_=ck rail to move outward as the train
passed over that spot, spreading the rail and causing the flange of the wheels
to go between the switch point and the st,ck rail. The Claimant, who had one
and one-half years experience as a Section Foreman, did not take into account
the tremendous lateral pressures on a curve which would exceed the normal
pressures exerted on the rail caused by a train consisting of 3 locomotive
units, 50 loads and 29 empty cars having a total weight of roughly 5,000 tons.
The record establishes that the Carrier has satisfied its burden of
proving that the claimant violated Circular 15, Rules G and F by failing to
observe "any deficiencies requiring attention" and failing to "take appropriate
action", resulting in unsafe track conditions, causing the derailment of Train
142. The record does not support the conclusion that the derailment was due to
a chipped or damaged switch point and stock rail, or to "something" that "fell
from or dropped from the train."
The Carrier has indicated that the Claimant has not been banned
forever from regaining his Foreman's seniority but will be re-evaluated at such
time to determine whether he has "gained the benefits of rehabilitation and
experience to warrant returning his Foreman's rights." In any event, it is the
Board's judgment that the discipline should not be disturbed.
Award Number 25012
Docket Number MW-24982
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FINDINGS: The Third Division of the Adjustment Board, upon the whole record and
all the evidence, finds and holds:
That the parties waived oral hearing;
That the Carrier and the Employes involved in this dispute are
respectively Carrier
and Employes within the meaning of the Railway Labor Act,
as approved June 21, 1934;
That this Division of the Adjustment Board has jurisdiction over the
dispute involved herein; and
That the Agreement was not violated.
A W A R D
Claim denied.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Third Division
ATTEST:
Nancy J er - Executive Secretary
Dated at Chicago, Illinois, this 26th day of September 1984.