NATIONAL RAILROAD ADJUSTMENT BOARD
THIRD DIVISION Docket Number CL-25743
Eckehard Muessig, Referee
(Brotherhood of Railway, Airline and Steamship Clerks
(Freight Handlers, Express and Station Employes
PARTIES TO DISPUTE:
(Terminal Railroad Association of St. Louis
STATEMENT OF CLAIM: "Claim of the System Committee of the Brotherhood
(GL-9916) that:
1. Carrier violated the Clerks' Rules Agreement when it
assessed discipline of fifteen (15) days deferred suspension to Crew
Board Clerk, Mr. R. T. Williams on January 12, 1984.
2. Carrier's action was harsh, excessive and unreasonable
due to the facts involved.
3. Carrier shall now be required to remove the fifteen (15)
day deferred suspension and all references thereto, from claimants
personal record, due to their harsh and unreasonable action."
OPINION OF BOARD: Subsequent to an investigation held on January 5, 1984,
in connection with the Claimant's alleged failure to
properly perform his duties as Crew Clerk, he was found guilty of mishan
dling a vacancy on the third shift, December 27, 1983, because he did
not follow established board marking procedure and, thus erred in marking
the board. The Carrier assessed a fifteen (15) day suspension to be
held in abeyance unless the Claimant would be disciplined again for a
similar offense prior to March 13, 1984.
The Organization contends that the notice of investigation
was procedurally defective, in that it stated that the position involved
had assigned hours commencing at 11:00 P. M., rather than the correct
hour of 10:30 P. M. The Board does not find this error prejudicial to
the Claimant. The record shows that he knew what the charge was and
was able to adequately prepare a defense.
Turning to the merits, on the basis of the record it cannot
be said that the Carrier lacked grounds for disciplinary action. However,
in this instance, there are factors which mitigate the gravity of the
offense. in this respect, the Board particularly notes that, while the
Claimant cannot completely absolve himself of responsibility for the
delay in filling the Crest Retarder Foreman assignment (the position in
question here), the record shows that there were others involved in the
events and occurrences that led to the error who also shared a degree
of responsibility. Moreover, it is apparent from reading the testimony
that there was some confusion as to the procedures and process to be
followed by those involved in the work associated with the Crew Board.
Award Number 25697 Page 2
Locket Number CL-25743
The Board finds these factors to be mitigating and, accordingly,
under all of the facts and circumstances, the discipline assessed was
harsh. Consequently, we shall reduce it to a five (5) day suspension
to be held in abeyance unless the Claimant was disciplined for a similar
offense prior to March 13, 1984.
FINDINGS: The Third Division of the Adjustment Board, upon the whole record
and all the evidence, finds and holds:
That the parties waived oral hearing;
That the Carrier and the Employes involved in this dispute
are respectively Carrier and Employes within the meaning of the Railway
Labor Act, as approved June 21, 1934;
That this Division of the Adjustment Board has jurisdiction
over the dispute involved herein; and
That the discipline was excessive.
A W A R D
Claim sustained in accordance with the Opinion.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Third Division
Attest
Nancy J. Dever - Executive Secretary
Dated at Chicago, Illinois, this 14th day of November 1985.
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