Form 1 NATIONAL RAILROAD ADJUSTMENT BOARD Award No. 27832
THIRD DIVISION Docket No. MW-26469
89-3-85-3-190
The Third Division consisted of the regular members and in
addition Referee Dana E. Eischen when award was rendered.
(Brotherhood of Maintenance of Way Employes
PARTIES TO DISPUTE:
(The Monongahela Railway Company
STATEMENT OF CLAIM: "Claim of the System Committee of the Brotherhood that:
(1) The discipline [thirty (30) days suspension from service deferred
for one year and a five (5) year disqualification for positions of foreman or
those requiring operation of on-track vehicles] imposed upon Track Patrol
Foreman P. P. Nosky for alleged 'Violation of Monongahela Railway Book of
Operating Rules, General Rules A, B1-2, B1-6, B1-7 and T' and for alleged
'Violation of Monongahela Railway Block Clearance Rules 302, 318 and 319' was
without just and sufficient cause and in violation of the Agreement.
(2) Claimant P. P. Nosky shall be restored to his former position as
track patrol foreman with seniority as such unimpaired, his record shall be
cleared of the charges leveled against him and he shall be compensated for all
wage loss suffered."
FINDINGS:
The Third Division of the Adjustment Board upon the whole record and
all the evidence, finds that:
The carrier or carriers and the employe or employes involved in this
dispute are respectively carrier and employes within the meaning of the
Railway Labor Act as approved June 21, 1934.
This Division of the Adjustment Board has jurisdiction over the
dispute involved herein.
Parties to said dispute were given due notice of hearing thereon.
As of December, 1983, Claimant was working as a Track Patrol Foreman,
7 A.M. to 3:30 P.M. On December 22, 23 and 30, 1983, he left work early, due
to illness or family problems, without obtaining permission or even notifying
his Supervisor. Notwithstanding his early quit on each of these days, Claimant put in for a full eig
December 30, 1983, Claimant left the patrol truck sitting on the main track
until 1:32 P.M., even though his block clearance had expired at 1:00 P.M. and
he falsely had reported being in the clear of 12:32 P.M.
Form 1 Award No. 27832
Page 2 Docket No. MW-26469
89-3-85-3-190
Following due notice and Investigation, at which Claimant essentially
admitted the foregoing charges, but pleaded factors in mitigation, i.e.,
leaving early for illness and family difficulties and leaving the vehicle on
the track after expiration of the block clearance because he "knew no train
was coming." After considering the facts and Claimant's 17 year service record, Carrier imposed a de
This discipline was appealed on grounds that Carrier violated
procedural requisites in the conduct of the Hearing and that the discipline
was unnecessarily harsh and excessive. The primary objection is to the
transcript of Investigation which Carrier provided Claimant and his Representative. It is not disput
Hearing and the transcript therefore was less than perfect. Given the realities of this case, howeve
the Hearing and in subsequent conferences, we can find no fatal procedural
defect in this record. As to the quantum of discipline, it may be severe but
we cannot say that it is unreasonably harsh or arbitrary. In the circumstances presented here we mus
A W A R D
Claim denied.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Third Division
Attest:
ancy JI~Ver - Executive Secretary
Dated at Chicago, Illinois, this 13th day of April 1989.