Form 1 NATIONAL RAILROAD ADJUSTMENT BOARD Award No. 28119
THIRD DIVISION Docket No. MW-27837
89-3-87-3-405
The Third Division consisted of the regular members and in
addition Referee John E. Cloney when award was rendered.
(Brotherhood of Maintenance of Way Employes
PARTIES TO DISPUTE:
(The Kansas City Southern Railway Company
STATEMENT OF CLAIM: "Claim of the System Committee of the Brotherhood that:
(1) The Agreement was violated when the Carrier used KCS Division
B&B forces to perform B&B work on the L&A Division seniority district on
December 11, 18, 19, 20, 21, 22, 23, 26 and 27, 1985 (Carrier's File
013.31-345).
(2) Messrs. H. H. Hoose, E. Jackson, C. D. Love, M. L. Cryer and
J. D. Wells shall each be allowed thirty (30) hours of pay at their respective
straight time rates and seventy-two and one-half (72 1/2) hours of pay at
their respective overtime rates because of the violation referred to in Part
(1) hereof."
FINDINGS:
The Third Division of the Adjustment Board upon the whole record
and all the evidence, finds that:
The carrier or carriers and the employe or employes involved in this
dispute are respectively carrier and employes within the meaning of the
Railway Labor Act as approved June 21, 1934.
This Division of the Adjustment Board has jurisdiction over the
dispute involved herein.
Parties to said dispute waived right of appearance at hearing thereon.
Claimants are members of B & B Gang 696 and their seniority is
restricted to Carrier's Louisiana & Arkansas Seniority District. This is a
pay claim for December 11, 18, 19, 20, 21, 22, 23 and 26 and 27, 1985, made on
January 12, 1986. The Organization alleges Carrier assigned B & B Gangs 691
and 692, whose seniority is limited to Carrier's Kansas City Southern District, to perform repair wo
within the Louisiana & Arkansas District.
On February 27, 1986, Carrier responded:
Form 1 Award No. 28119
Page 2 Docket No. MW-27837
89-3-87-3-405
"KCS Bridge Gang 692, with 2 members of KCS
Bridge Gang 691 assisting them, worked their
entire work shift on December 11, 1985 repairing
KCS Bridge A-540 and on December 18, 1985 worked
their entire work shift loading a car with Company material at Texarkana, Texas. B&B 692,
again with 2 members of B&B 691, worked on L&A
Bridge B-99.8 on December 19, 1985, ten hours
straight time and 1 1/2 hours overtime; on
December 20, 1985 10 hours straight time and
1 1/2 hours overtime; on December 21, 1985 12
hours overtime; on December 22, 1985 11 1/2
hours overtime; on December 23, 1985 12 hours
overtime; on December 26, 1985 10 hours straight
time; and on December 27, 1985 10 hours straight
time.
Some time prior to claim dates a contractor
working for the State of Louisiana began dredging the Flat River, which flows under L&A Bridge
B-99.9. The contractor exceeded reasonable
excavation under the bridge and it began to
collapse. By December 19, 1985 some of the
piling had come out from under the caps and we
were faced with the probability of losing the
entire bridge in a matter of hours. The main
line was taken out of service and, because of
the extreme emergency, KCS Bridge Gang 692, with
2 men from KCS Bridge Gang 691, were rushed to
the site to commence operations to save the
bridge. The KCS Bridge gang was available in
the immediate area whereas LSA Bridge Gang 696
was located some 250 miles away, thus requiring
a full day's travel to reach the site of Bridge
B.99.8. We very well could have lost the bridge
while B&B 696 was on the road."
The Organization did not challenge Carrier's contention that the main
line was taken out of service or that substantial amounts of overtime hours
were worked by the assigned crews. Neither did it contest Carrier's assertion
that the KCS Gang had actually worked on KCS Bridge A-540 on December 11,
1985, and loaded cars at Texarkana, Texas on December 18, 1985, rather than
working at Adner as claimed. The Organization did inquire why the days worked
were non-consecutive if an emergency existed but this question went unanswered.
In progressing the Claim on first and second appeal, the organization
referred to dates in 1986, rather than 1985. The claim presented to this
Board again refers to 1985. Carrier argues the Claim is therefore procedurally defective. We disagre
with the Claim filed on January 12, 1986. We do not consider the obvious
typographic errors in subsequent correspondence fatal. At all times the
parties knew the nature and extent of the Claim as well as the dates of the
Incident out of which it arose.
Form 1 Award No. 28119
Page 3 Docket No. MW-27837
89-3-87-3-405
The Organization contends Carrier did not establish an emergency
existed. It cites cases holding emergencies are sudden, unforeseeable events
that bring operations to an immediate halt. However emergencies are not confined to Acts of God or s
into disaster. Here Carrier asserted it had to take the main line out of
service and was faced with the possibility of losing the bridge as a result of
actions of employees over which it had no control. This is not rebutted.
Faced with this situation it was not unreasonable of Carrier to assign a gang
in the immediate area rather than one over 250 miles away. Carrier's position
that it was responding to an emergency is also supported by the fact that
Gangs 691 and 692 were apparently assigned on December 19, 1985, the date
Carrier contends the possibility of loss of the bridge arose rather than
December 11 and 18, 1985, as claimed by the Organization. The failure to work
the gang consecutive days may raise a question, but significant overtime was
worked in the three days before Christmas Eve and Christmas Day. We hold
Carrier, faced with what it reasonably perceived to be an emergency, did not
violate the Agreement by making the assignment at issue.
A W A R D
Claim denied.
NATIONAL RAILROAD ADJUSTMENT BOARD
By Order of Third Division
Attest:
Nancy J er~- Executive Secretary
Dated at Chicago, Illinois, this 25th day of September 1989.