Form 1 NATIONAL RAILROAD ADJUSTMENT BOARD
THIRD DIVISION
Award No. 32121
Docket No. SG-32833
97-3-96-3-159

The Third Division consisted of the regular members and in addition Referee John H. Abernathy when award was rendered.


PARTIES TO DISPUTE:
(CSX Transportation, Inc. (former Louisville and
( Nashville Railroad Company)

STATEMENT OF CLAIM:



FINDINGS:

The Third Division of the Adjustment Board, upon the whole record and all the evidence, finds that:

The carrier or carriers and the employee or employees involved in this dispute are respectively carrier and employee within the meaning of the Railway Labor Act, as approved June 21, 1934.
Form 1 Award No. 32121
Page 2 Docket No. SG-32833
97-3-96-3-159

This Division of the Adjustment Board has jurisdiction over the dispute involved herein.




On February 16, 1995, two Carrier Supervisors began inspecting signals, crossing gates, etc. on Claimant's assigned territory near New Orleans, Louisiana. Numerous serious FRA defects were found. Claimant was removed from service that day after having worked six hours.


The next day, February 17, Claimant willingly participated in a further inspection of his territory conducted by the Supervisors. Additional defects, many of which were considered unsafe for both rail and passenger traffic, were found. Claimant was questioned on February 17 about those defects, but did not provide acceptable reasons for the defects.


Charges were brought against Claimant on February 21, 1995 for "unsafe maintenance practices." A formal Investigation was scheduled and conducted on February 28, 1995. After this Investigation was complete, Carrier determined it had sufficient probative evidence to find Claimant guilty of the charge. As a penalty, Carrier assessed a 30 day suspension.


The Organization appealed the Carrier's decision claiming the Investigation was not held within ten days of the date the Claimant was first removed from service (February 16); that Claimant did not receive 48 hours advanced notice of the charges; that the charges lacked specificity; and that the Carrier failed to meet its burden of proving the Claimant was responsible for the maintenance defects on his territory.


The Board reviewed the record and has come to the following conclusions. First, the Claimant was not surprised or misted by the charge levied against him. Defects were verbally pointed out to the Claimant and discussed with him on both February 16 and 17 by the Supervisors. Those specific defects formed the basis of the general charge of unsafe maintenance practices. Second, Claimant was afforded a fair and impartial Hearing on those unsafe practices and was given an opportunity to respond to them. Third, Rule 55 requires an Investigation to be held within ten days of the charge date .Qr the date the employee is withheld from service. Claimant was withheld from service on February 16 and charged on February 21. The Investigation was held on February

Form 1 Award No. 32121
Page 3 Docket No. SG-32833



28 - 12 days after the withheld from service date, but seven days after the charge date. The Board finds the Investigation was timely held within ten days of the charge date in accordance with Agreement Rule 55. Fourth, the record contains substantial evidence of Claimant's guilt of maintenance defects and practices.


Finally, these are serious offenses. It is undisputed that a faulty signaling system could cause an accident with a high potential for loss of life and property. The assessment of a 30 day suspension for such a serious matter is justified and proper in this case.


                        AWARD


      Claim denied.


                        ORDER


This Board, after consideration of the dispute identified above, hereby orders that an award favorable to the Claimant(s) not be made.


                      NATIONAL RAILROAD ADJUSTMENT BOARD

                      By Order of Third Division


Dated at Chicago, Illinois, this 13th day of August 1997.