AWARD N0. 187
Case No. 221
PUBLIC LAW BOARD N0. 1582
PARTIES) ATCHISON, TOPEKA AND SANTA FE RAILWAY COMPANY
TO )
DISPUTE) BROTHERHOOD OF MAINTENANCE OF.WAY EMPLOYEES
STATEMENT OF CLAIM
:
1. That the Carrier's decision to assess Southern Division Foreman
E. J. McDade's record with thirty (30) demerits as a result of investigation held at Temple, Texas April 5, 1982 was injust.
2. That the Carrier now, expunge thirty (30) demerits from claimant
McDade's personal record and compensate for wage loss and expenses
incurred as result of him attending the investigation April 5, 1982,
because the record 'does not contain substantial evidence that claimant McDade violated the Carrier's rules named in the Notice of Investigation and even if claimant violated rules as alleged the
assessment of thirty (30) demerits is harsh and excessive discipline.
FINDINGS: This Public Law Board No. 1582 finds that the parties
er~are Carrier and Employee within the meaning of the Railway
Labor Act, as amended, and that this Board has jurisdiction.
In this dispute the claimant was charged with allowing Mykawa Road
Switcher Engine #2227 to use turnout portion of Betz lab switch with
guard rail not securely fastened, allowing the R4 to climb the frog
point, derailing
the lead end of Engine #2227 on March 15, 1982 near
Mykawa, Texas. An investigation was held, and pursuant thereto the
claimant was assessed 30 demerits.
The conductor on Road Switcher #2227 testified that he observed the
guard rail immediately after the car derailed and that he went underneath the car to determine why it had derailed and saw a gap between
the rail and the guard rail of about one and one-half inches on the
lead end where the car approached it..
The conductor also testified there was a bolt in the guard rail laying between the two rails on the ties, and it
certainly was not in
place. He also testified that the switch was unsafe although the
claimant had advised him that it was safe.
Assistant Division Engineer G. W. Beattie testified that he discussed
the incident with the claimant who advised him that someone had removed the bolt from the guard rail, but later the claimant changed
his story and said there was definitely a bolt in the guard rail but
it was loose. He further testified that he request that the guard
/,Sga Award No. 187
Page 2
rail clearance be measured, and it was found there was two and
one-half inches of clearance.
The claimant testified that he was in charge of the switch, that
the switch was new and did have a bolt in it, but the bolt was not
quite tight but was slightly loose. The claimant contended that
the loose guard rail was not the cause of the derailment.
However, Assistant Division Engineer Beattie was questioned in
this regard, and he testified there were definite marks indicating
that the car climbed the point of the frog.
The Board has carefully reviewed the testimony of record and finds
there is no justification'for setting'the discipline aside.,
AWARD: Claim denied.
~ restore . Moore, Ct`a
rgaa zat .oa Mem er
Dated at Chicago, Illinois
Mar
26: 1982 ..