At the investigation held on February 1, 1982, the District General Foreman
and the Section Foreman at Keddie testified that on January 24, 1982, they
thoroughly examined the track where the derailment occurred. They found the
track gauge had expanded by approximately two inches which allowed the trucks
to fall inside the rail. Both officials observed that all ballast had been
removed from the cribs (between the ties) though ballast remained around the
ends of the ties. In addition, for a span of seventeen and one-half feet,
the ties were disconnected from the rails. Based on their experience, the
General Foreman and Section Foreman theorized that the Section Gang assigned
to maintain track in the area had removed the ballast from the cribs in
anticipation of changing out the ties and pouring in new ballast. The absence
of ballast in the cribs left the ties and rails unsupported so as trains moved
over the track, the ties gradually loosened and became disengaged from the