PARTIES TO THE DISPUTE:
Brotherhood of Maintenance of Way Employees
and
Chicago and North Western Transportation Company
STATEMENT OF CLAIM:
Claire of the System Committee of the Brotherhood that:
(1) The dismissal of Track Foreman D. L. Switzer, effective on
February 25, 1977, was without just
and
sufficient cause
and based upon unproven charges.
(2) Mr. Switzer be reinstated with all rights unimpaired and
paid for all time lost because of the violation referred
to within Part (1) hereof. .
OPINION OF BOARD:
.Claimant entered Carrier's service in 1948 and was promoted to Foreman
in 1956. Track Foreman Switzer was dismissed from service effective
February 25, 1977 following a hearing and investigation. into charges
reading as follows:
Your violation of Rule 1241 on Monday, January 31,
1977, between Elkton and Taopi, Minnesota as prescribed in Rules of Engineering Department, C&NW
Railway Company as follows:.
Sec. Foreman must carefully inspect rail
for defects or breaks and remove all
defective rail as soon as possible.
On Monday, January 31, 1977, Claimant and his crew were performing'
track work on the Oelwein Subdivision of Carrier's Central Division. A
defective rail with a head and web separation was found. In replacing
2
that defective rail Claimant had to cut the replacement rail to the proper
As replacement rail he
used
apiece of rail which had been removed
from the track about one week earlier due to a bolt hole defect. Claimant
began to cut the replacement rail to the proper length using an abrasive
saw to cut off the end with the bolt hole defect. The saw did not work
properly and Claimant finished the cut with a cutting torch. Engineering
Department Rules permit cutting rails with a cutting torch but only for
use on side track or in yards or for temporary cuts on main lines. Temporary
replacements of rail in such situations must be accompanied by a ten-mile per
bour slow order. Claimant finished the cutting job with the torch and
Installed the replacement rail. 8e did not notice any defects and did not
put a ten-mile per hour slow order over the rail. The next day, February 1,
1977, a train proceeded over the replaced rail at timetable speed and derailed
a unit and fifteen cars.
Evidence adduced at the hearing showed that the derailment was caused
because the replacement rail had a vertical split head. It is apparent from
the hearing record that the split head was not evident at the time of installation by looking down on the ball of the rail but was detectable by close
examination of the torch cut end. Following the derailment the vertical
split head in the replacement rail was plainly visible.
A careful review of the record in our judgment supports Carrier's conclusion that Claimant did not give the replacement rail the kind of thorough
inspection required by Rule 1241. Specifically, the record persuades us
that he examined the rail by looking down on the ball of the rail but did
not thoroughly inspect the ends, especially the torch cut end. We should
point out that we do not find convincing the suggestion of Carrier that the
torch cutting caused the defect; but we are persuaded that Claimant failed
to make the kind of thorough inspection which might have found the defect.
3
y
Although not specifically charged with sans, Claimant admitted at the
hearing that he violated another rule by not putting a ten-mile per hour
slow order on
the section of
main lire ieplaced by the
torch cut rail.
We
cannot concur with the
Organizations's position
that Claimant's due process
rights were violated: when.: he vas found qty of violating that rule - as
well as Rule 1241. Claimant freely admitted.the slow order transgression
and his culpability thex6' is so interir:oven. with the 'failure .to
properly inspect the rail that we cannot concur in the
Organization's view
that they hearing amounted: to a
"fishing
expedition." Additionally,
we note
that ,Claimant's asions
are
reiterated: by the Organization in appeal
letters on the property
reading
in pertinent part as follows:
Mr. Bwitzex used.poor judgment when he failed to place
a 10 mile per~hour
speed:
restriction on this section
of track. This is the only violation for which he
could have been: charged:
Dismissal of a 29 year employee'.might well
be deemed excessive `.
discipline.. But shortly after.
he
vas terminated. Claimant took his Railroad
Retirement Annuity, effective April
11
1977. By that action he rendered.
the claim for reinstatement mot and the
claim
for
compensation for all
time lost was limited- to
the period
February 25; 1977 to March 31, 1977,
the last day before :his Annuity became effective.
In
effect Claimant's
retirement makes: this a -de,facto suspension of.35 days without pay rather:
than
a dismissal.
We cannot
find
that
a
suspension of 35 days is
arbitrary, unreasonable or
capricious _ given
the proven violation of work
rules. Accordingly, the discipline assessed is reduced. for the record to
a
35-day suspension.
Public Law Board No. 1844, upon the whole record and all of the
evidence,. finds
and holds as follows:
That the Carrier, and
Employee involved in this dispute are,
respectively, Carrier-and Employee within the meaning of the Railway Labor
Act; .
2. that the Board has jurisdiction over. the dispute involved
herein=
and
that
the dismissal was excessive.
Claim, sustained. to the extent
indicated 'in the opinion.
Dana E. Eischen, Cha.irr_.---'
Fi. G. Harper, Employed. member
R, iii. Scrmiege, . Carrier Member
Dated: December Fi, 1978 -